PERMIAN RESOURCES, LLC UL Daily Drilling Partner Summary

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1 PRES WELL NO. Report End Date: 5/19/2016 Report Number: 3 Rig: INTEGRITY, 3 Projected Days (days): 0 Drilling Days: : : 0 Planned VS (ft): Current VS (ft): WOC WOC, CONTACTED TRRC, SPOKE TO ABRAHAM, ADVISED TO 1in CEMENT TO SURFACE. CUT OFF CASING, RIH W/ 1in PIPE AND ATTEMPTED TO PUMP CEMENT TO SURFACE. NO RETURNS. WOC FOR 8 HOURS. RIH W/ 1in PIPE AND ATTEMPTED TO PUMP CEMENT TO SURFACE. NO RETURNS. WOC FOR EIGHT HOURS. RIH W/ 1in PIPE AND ATTEMPTED TO PUMP CEMENT TO SURFACE. NO RETURNS. 0 WOC FOR EIGHT HOURS AND RIH FOR TOP OUT JOB. 05:00 07: WOC. SURF VERT DRILL WAIT ON CEMENT No 07:00 08: RU VES AND RUN TEMP LOG. TOC FOUND AT 200ft SURF VERT DRILL DIRECTIONAL WORK No 08:30 09: CUT OFF CASING, RUN 1in PIPE, RIG UP CEMENTERS SURF VERT DRILL RIG UP/RIG DOWN No 09:30 10: RIG UP CREST CEMENTERS AND PUMP 20bbls H2O, 20bbls H2O w/cacl, 24bbl CLASS C PREM PLUS, NO RETURNS. SURF VERT DRILL RUN CEMENT No 10:30 18: WOC. SURF VERT DRILL WAIT ON CEMENT No 18:30 19: RIG UP CREST CEMENTERS 20bbls H20 WITH CALCIUM CHLORIDE. PUMPED 20bbls (100sx) CLASS C PREMIUM PLUS CEMENT DOWN THE BACKSIDE OF THE CASING. NO RETURNS. SURF VERT DRILL RUN CEMENT No 19:30 03: WOC. SURF VERT DRILL WAIT ON CEMENT No 03:30 05: RIG UP CREST CEMENTERS 25bbls H20 WITH CALCIUM CHLORIDE. PUMPED 36bbls (150sx) CLASS C PREMIUM PLUS CEMENT DOWN THE BACKSIDE OF THE CASING. NO RETURNS. SURF VERT DRILL RUN CEMENT No

2 PRES WELL NO. Report End Date: 5/20/2016 Report Number: 4 Rig: INTEGRITY, 3 Projected Days (days): 0 Drilling Days: : : 0 Planned VS (ft): Current VS (ft): RELEASED RIG. WOC, RUN TEMP SURVEY, FOUND ESTIMATED TOP AT 70ft, RIH W/ 1in PIPE AND CEMENT WITH 200sxs, NO RETURNS. WOC FOR 8 HOURS, CEMENTED TO SURFACE WITH GROUT TRUCK. WAIT ON BIG RIG. RD AND RELEASE RIG AT 00:30 ON 5/20/ :00 11: WOC. SURF VERT CSG/CEMENT WAIT ON CEMENT No 11:30 12: RU VES AND RUN TEMP LOG. ESTIMATED TOC AT 70ft. SURF VERT CSG/CEMENT DIRECTIONAL WORK No 12:00 16: RIG UP CREST CEMENTERS 25bbls H20 WITH CALCIUM CHLORIDE. PUMPED 47bbls (200sx) CLASS C PREMIUM PLUS CEMENT DOWN THE BACKSIDE OF THE CASING. NO RETURNS. RELEASE CEMENTERS AND CALLED GROUT TRUCK. SURF VERT CSG/CEMENT RUN CEMENT No 16:00 00: WOC. SURF VERT CSG/CEMENT WAIT ON CEMENT No 00:00 02: RU GROUT TRUCK AND POUR DOWN BACKSIDE OF CASING. SUCCESSFUL TOP OUT WITH 1.7 YARDS OF GROUT TO SEE RETURNS. SURF VERT CSG/CEMENT RUN CEMENT No 02:00 02: RIG DOWN AND RELEASE RIG. SURF VERT CSG/CEMENT RIG UP/RIG DOWN No

3 Report End Date: 5/27/2016 Report Number: 5 Drilling Days: : : 0 Planned VS (ft): Current VS (ft): PERFORM MAINTENANCE ON RIG MOVE CAMP, DRILL PIPE AND MISC EQUIPMENT TO UNIVERSITY PAD WHILE RIG DOWN ENSIGN 786 MOVE ENSIGN 786 TO UNIVERSITY PAD MIRU ON 70% RIGGED DOWN, 50% MOVED. 10% RIGGED UP 24 HOURS FROM RIG RELEASE. LAST SURVEY: 600 ft. MD,.76 INC, 312 AZM. ( GYRO ) 0 05:00 17: RIG DOWN ON THE WOODS RE HA, MOVE DRILL PIPE, CO. TRAILERS, AND MISC. EQUIPMENT TO NEW LOCATION, LOWERED SUB AND DERRICK AT 1300 hrs MOB MOB MOB RIG UP/RIG DOWN No 17:00 05: PRESSURE WASH DERRICK AND SUB, PERFORM RIG MAINTENANCE MOB MOB MOB RIG UP/RIG DOWN No

4 Report End Date: 5/28/2016 Report Number: 6 Drilling Days: : : 0 Planned VS (ft): Current VS (ft): RIGGING UP MIRU ON, LOAD OUT AND SET SUBS, PITS, MOTOR PACKAGE AND MISC RIG EQUIPMENT MIRU ON 100% RIGGED DOWN, 95% MOVED. 25% RIGGED UP 48 HOURS FROM RIG RELEASE. EST SPUD: MONDAY AM LAST SURVEY: 600 ft. MD,.76 INC, 312 AZM. ( GYRO ) 0 RAISE DERRICK, SKID RIG TO, FINISH SETTING IN RIG, CONTINUE RU AND RU THIRD PARTY EQUIPMENT. 05:00 18: MIRU ON, SET MATS AND SUBS,INSTALLED CENTER SECTION,WALKING FEET, DRAWWORKS, DIESEL AND WATER TANKS MOB MOB MOB RIG UP/RIG DOWN No 18:00 05: INSTALL DERRICK ON SUB, STRING UP, WIRED UP DRAWWORKS, PLUMBED IN CENTER SECTION,RIGGED UP SHALE SHAKER, WIRED UP MUD PUMPS, CHANGE LIGHTS ON DERRICK MOB MOB MOB RIG UP/RIG DOWN No

5 Report End Date: 5/29/2016 Report Number: 7 Drilling Days: : : 0 Planned VS (ft): Current VS (ft): RIGGING UP MIRU ON, DISCOVERED CRACK IN BEAM ON DERRICK WHILE REPLACING LIGHTS, WAIT ON TYPE A 572 GRADE 50 METAL AND WELDER TO REPAIR DRILLER SIDE SUPPORT BEAM IN DERRICK, REPAIR BEAM IN DERRICK, RIG UP MISC RIG EQUIPMENT, CERTIFICATION OF DERRICK REPAIR IS PENDING MIRU ON 100% RIGGED DOWN, 100% MOVED. 30% RIGGED UP 72 HOURS FROM RIG RELEASE. EST SPUD: MONDAY PM LAST SURVEY: 600 ft. MD,.76 INC, 312 AZM. ( GYRO ) 0 RAISE DERRICK, SKID RIG TO, FINISH SETTING IN RIG, CONTINUE RU AND RU THIRD PARTY EQUIPMENT. 05:00 15: WHILE PERFORMING DERRICK INSPECTION, MOTORMAN DISCOVERED CRACK IN DRILLER SIDE SUPPORT BEAM IN DERRICK AND REPORTED TO TOOL 0600 hrs, ENSIGN MANAGMENT WAS NOTIFIED AND REPAIRS DETERMINED BY ENSIGN ENGINEER AND WOOLSLAYER (DERRICK MANUFACTURER) CONTINUED CRANE WORK UNTIL 9 AM. PERFORMED MISC RIG UP AS FOLLOWS WHILE WAIT ON DERRICK REPAIRS MOB MOB MOB RIG UP/RIG DOWN Yes SET GAS SEPARATOR, HOOKED UP WATER LINES TO SKID, FLIPPED BLOCK ON CHOKE MANIFOLD, PUT CAMERA IN DERRICK, SET MATS FOR POLHY LINE FROM FRAC TANK TO MUD PITS. 15:00 05: WELDED CRACK IN DERRICK, INSTALLED TYPE A 572 GRADE 50 METAL PATCH ON BEAM IN DERRICK AND WELDED SAME. HI TECH PERFORMED MPI. WAITED ON APPROVAL FROM WOOLSLAYER AND ENSIGN ENGINEER, PERFORMED MISC RIG UP AS FOLLOWS WHILE WAITING ON DERRICK REPAIRS : FINISHED WITH MPI OF DERRICK REPAIR AT 2200 HRS. MOB MOB MOB RIG UP/RIG DOWN Yes INSPECTED #2 MUD PUMP, INSPECTED LIGHT IN DERRICK, SPOTTED WATER FRAC TANKS, LAYED OUT HOSES FOR JET LINES NOTE : CERTIFICATION OF DERRICK REPAIR IS PENDING

6 Report End Date: 5/30/2016 Report Number: 8 Drilling Days: : : 0 Planned VS (ft): Current VS (ft): RIGGING UP MIRU ON, RIG UP, RAISED DERRICK AND RIG FLOOR, INSTALLED WALKING FEET, DRESSED OUT RIG FLOOR, SKID RIG TO UNIVERSITY UNIT RE HK, CONTINUED R/U MIRU ON 100% RIGGED DOWN, 100% MOVED. 60% RIGGED UP 96 HOURS FROM RIG RELEASE. EST SPUD: TUESDAY AM LAST SURVEY: 600 ft. MD,.76 INC, 312 AZM. ( GYRO ) 0 CONTINUE RU AND RU THIRD PARTY EQUIPMENT. 05:00 08: PERFORMED MISC RIG UP; RECEIVED APPROVAL TO RAISE DERRICK AND CONTINUE DRILLING OPERATIONS AT 0730 hrs MOB MOB MOB RIG UP/RIG DOWN Yes 08:00 08: RAISED DERRICK AND PINNED SAME MOB MOB MOB RIG UP/RIG DOWN No 08:30 10: INSTALLED FRONT WALKING FEET, INSTALLED RAISING CYLINDERS, INSTALLED FLOOR PLATES, HANDRAILS, AND DRILLERS' CONSOLE MOB MOB MOB RIG UP/RIG DOWN No 10:30 11: RAISED RIG FLOOR AND PINNED SAME MOB MOB MOB RIG UP/RIG DOWN No 11:00 13: INSTALLED DOGHOUSE, LOWERED MAST CYLINDERS, INSTALLED FLOOR PLATES, STAIRS AND HANDRAILS, SHIMMED IRON ROUGHNECK 13:30 18: SPOTTED CHOKE MANIFOLD, HP UNIT, KOOMEY, WRANGLER, CATWALK, AND INSTALLED FLOWLINE, WIRED UP TOP DRIVE AND IRON ROUGHNECK 18:30 23: TRANSFERED OBM TO PITS, INSTALLEDCHOKE LINES TO GAS BUSTER, FLOW LINE, AIR LINES 23:00 05: INSTALLED CHOKE LINES, MUD LINES, WORKED ON AIR HOIST AND R/U KOOMEY TO RIG FLOOR MOB MOB MOB RIG UP/RIG DOWN No MOB MOB MOB RIG UP/RIG DOWN No MOB MOB MOB RIG UP/RIG DOWN No MOB MOB MOB RIG UP/RIG DOWN No

7 Report End Date: 5/31/2016 Report Number: 9 Drilling Days: : : 0 Planned VS (ft): Current VS (ft): TESTING BOP'S MIRU ON, CONTINUED RIGGING UP, PERFORMED SPIN AND TORQUE TESTS ON TOP DRIVE,NIPPLED UP BOP AND TESTED SAME 100% RIGGED DOWN, 100% MOVED. 100% RIGGED UP 120 HOURS FROM RIG RELEASE. EST SPUD: TUESDAY PM LAST SURVEY: 600 ft. MD,.76 INC, 312 AZM. ( GYRO ) 0 FINISH TESTING BOP, N/U FLOWLINE,INSTALL TARP ON POLLUTION PAN,INSTALL WEARBUSHING, P/U DIRECTIONAL B.H.A.,T.I.H. ( TAG ) DISPLACE WBM WITH 9.2 PPG. OBM, DRILL OUT SHOE TRACK, DRILL 12 1/4" INTERMEDIATE HOLE SECTION AS PER APROVED DIRECTIONAL PLAN # 1 05:00 08: HOOKED UP SERVICE LINES TO RIG FLOOR MOB MOB MOB RIG UP/RIG DOWN No 08:00 16: TESTED DRAWWORKS - DRUM WOULD NOT MOVE, TROUBLE SHOT SAME, CHANGED OUT 3 WAY ACTUATOR VALVE, AND TRANSDUCER; FUNCTIONED IRON ROUGHNECK, CATWALK, WELDED PASON FLOWLINE SENSOR ADAPTOR ONTO FLOWLINE, INSTALLED DRAIN HOSES, SET OUT GERONIMO LINE, RAN FILL UP LINE 16:00 18: SPOOLED UP DRAWWORKS, PUT WRAPS ON DEADMAN, UNPINNED BLOCKS F/DERRICK 18:30 20: FUNCTION TESTED TOP DRIVE HYDRAULICS, INSTALLED SAVER SUB AND FEATHER RING MOB MOB MOB RIG UP/RIG DOWN Yes MOB MOB MOB RIG UP/RIG DOWN No MOB MOB MOB RIG UP/RIG DOWN No 20:30 00: PERFORMED TOP DRIVE SPIN TEST AND TORQUE TEST MOB MOB MOB RIG UP/RIG DOWN No 00:00 03: INSTALLED B.O.P.'S ON WELLHEAD, INSTALLED CHOKE LINE AND TORQUED SAME WITH " MCE", TESTED BACK TO PUMPS 250 psi 5 min AND 4000 psi/5 min. TESTED CHOKE MANIFOLD 250 psi/5 min AND 5000 psi/5 min ( OFF LINE ), CASING TESTED TO 1,150 PSI BY SPUDDER RIG NOTE : RIG ACCEPTED TO DAYWORK AT 00:00 HRS. ON :00 05: PERFORMED ACCUMULATOR DRAW DOWN TEST,LD BOP WRANGLER,TESTING BOP AND RELATED EQUIPMENT. TESTING BLIND, BOTTOM AND TOP RAMS, KILL, MANUAL, FLOOR VALVES, WITH 250 psi/5 min AND 5000 psi/5 min. TESTING HYDRILL WITH 250 psi/5 min AND 3500 psi/5 min. MOB MOB MOB NIPPLE UP B.O.P./WELLHEAD MOB MOB MOB TEST B.O.P No No

8 Report End Date: 6/1/2016 Report Number: 10 Drilling Days: 1 : 1,750 : 1,075 Current VS (ft): 26 DRILLING 12 1/4" INTERMEDIATE HOLE SECTION TEST BOP, PICKED UP 12 1/4 BHA, TIH TO 635', DRILL OUT SHOE TRACK AND DRILL 12 1/4" INTERMEDIATE SECTION FROM ft. TO 1,750 ft., MW 9.3 PPG. LAST SURVEY: 1,641 ft. MD, 8.79 INC, AZM BEHIND, 7.6 LEFT, BOTTOM HOLE TEMP DISTANCE FROM : UNIVERSITY UNIT 1 RE HS - 31' UNIVERSITY UNIT 1 RE HA - 62' UNIVERSITY UNIT 1 RE HK - 135' 1,750 1,075 DRILL 12 1/4" INTERMEDIATE HOLE SECTION AS PER APROVED DIRECTIONAL PLAN # :00 06: PERFORMED ACCUMULATOR DRAW DOWN TEST,LD BOP WRANGLER,TESTING BOP AND RELATED EQUIPMENT. TESTING BLIND, BOTTOM AND TOP RAMS, KILL, MANUAL, FLOOR VALVES, WITH 250 psi/5 min AND 5000 psi/5 min. TESTING HYDRILL WITH 250 psi/5 min AND 3500 psi/5 min. MOB MOB MOB TEST B.O.P No 06:00 12: HOOK UP FLOWLINE, INSTALL TARP ON POLLUTION PAN, INSTALLED MOUSEHOLE, FLOWLINE, TURNBUCKLES, KILL LINE AND BLEED OFF LINE, INSTALL DRAIN LINES, INSTALL MUD BUCKET LINE MOB MOB MOB NIPPLE UP B.O.P./WELLHEAD 12:00 12: INSTALLED WEAR BUSHING MOB MOB MOB BOP/OTHER No 12:30 16: PICKED UP 8 in CATHEDRAL MUD MOTOR, 1.75 FIXED, 7/8 LOBE, 4.0 STAGE, WITH 11 in NEAR BIT STABILIZER, 12 1/4 in BAKER T606X BIT (SN ), 6X22 JETS, TFA 2.2, SCRIBED, INSTALLED AND PROGRAMMED EM TOOL MOB MOB MOB P/U & L/D BHA No 16:00 17: TIH, TAGGED CEMENT AT 635 ft. MOB MOB MOB TRIPS No 17:30 18: DISPLACED WBM IN HOLE WITH 9.3 ppg OBM WHILE DRILLING CEMENT AND SHOE TRACK FROM 635 ft TO ft. 18:00 23: ,239 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 765 ft TO 1,239 ft, 564 ft AT FPH ROTATE DRILLED : 519 ft IN 3.75 HOURS AT FPH AVERAGE ROP SLIDE DRILLED : 45 ft IN 1.25 HOURS AT 36 FPH AVERAGE ROP 92.0% ROTATE, 8.0% SLIDE FULL RETURNS - MW 9.3 *SPUD WELL ON AT 18:00 hrs* MOB MOB MOB DRILL W/ MUD No 23:00 23: ,239 1,239 PERFORMED RIG / TOP DRIVE SERVICE INT DIR DRILL LUBRICATE RIG No 23:30 05: ,239 1,750 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 1,239 ft TO 1,750 ft, 511 ft AT 92.9 FPH ROTATE DRILLED : 281 ft IN 1.75 HOUR AT FPH AVERAGE ROP SLIDE DRILLED : 230 ft IN 3.75 HOUR AT 61.3 FPH AVERAGE ROP 55% ROTATE, 45% SLIDE FULL RETURNS - MW 9.3 No

9 Report End Date: 6/2/2016 Report Number: 11 Drilling Days: 2 : 3,684 : 1,934 Current VS (ft): 409 DRILLING 12 1/4" INTERMEDIATE HOLE SECTION DRILL 12 1/4" INTERMEDIATE SECTION FROM 1750 ft. TO 3,684 ft., MW 9.4+ PPG. TARGET CHANGE; NEW TARGET 7984 KBTVD at 0'VS at INC at AZM LAST SURVEY: 3,521 ft. MD, INC, AZM. 8.8 AHEAD, 3.2 RIGHT, BOTTOM HOLE TEMP 124 DISTANCE FROM : UNIVERSITY UNIT 1 RE HS - 289' UNIVERSITY UNIT 1 RE HA - 320' UNIVERSITY UNIT 1 RE HK - 386' 1,750 3,684 1,934 DRILL 12 1/4" INTERMEDIATE HOLE SECTION AS PER APROVED DIRECTIONAL PLAN # :00 23: ,750 3,402 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 1,750 ft TO 3,402 ft, 1,652 ft AT 91.8 FPH ROTATE DRILLED : 1,566 ft IN 15.5 HOUR AT FPH AVERAGE ROP SLIDE DRILLED : 86 ft IN 2.5 HOUR AT 34.4 FPH AVERAGE ROP 95% ROTATE, 5% SLIDE FULL RETURNS - MW 9.3 TARGET CHANGE; NEW TARGET 7984 KBTVD at 0'VS at INC at AZM 23:00 23: ,402 3,402 PERFORMED RIG / TOP DRIVE SERVICE INT DIR DRILL LUBRICATE RIG No 23:30 02: ,402 3,568 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 3,402 ft TO 3,568 ft, 166 ft AT 55.3 FPH ROTATE DRILLED : 166 ft IN 3.0 HOUR AT 55.3 FPH AVERAGE ROP SLIDE DRILLED : 0 ft IN 0 HOUR AT FPH AVERAGE ROP 100% ROTATE, 0% SLIDE FULL RETURNS - MW 9.35 WELL STARTED FLOW ON CONNECTION AT 3,500 ft 02:30 03: ,568 3,568 CHANGE OUT ROTATING HEAD, GAINED 50 bbls WHILE CHANGING OUT ROTATING HEAD, WELL FLOWING AT 200 bbls hr. SHUT IN WELL AND WEIGHT UP TO 9.4 ppg, 03:30 05: ,568 3,684 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 3,568 ft TO 3,684 ft, 116 ft AT 77.3 FPH ROTATE DRILLED : 116 ft IN 1.5 HOUR AT 77.3 FPH AVERAGE ROP SLIDE DRILLED : 0 ft IN 0 HOUR AT 0 FPH AVERAGE ROP 100% ROTATE, 0% SLIDE FULL RETURNS - MW 9.4+ INT DIR DRILL BOP/OTHER Yes

10 Report End Date: 6/3/2016 Report Number: 12 Drilling Days: 3 : 5,481 : 1,797 Current VS (ft): 738 DRILLING 12 1/4" INTERMEDIATE HOLE SECTION DRILL 12 1/4" INTERMEDIATE SECTION FROM 3,684 ft. TO 5,481 ft., MW 9.4+ PPG. LAST SURVEY: 5,306 ft. MD, INC, 312 AZM. 9 BEHIND, 7 LEFT, BOTTOM HOLE TEMP 142 DISTANCE FROM : UNIVERSITY UNIT 1 RE HS - 542' UNIVERSITY UNIT 1 RE HA - 590' UNIVERSITY UNIT 1 RE HK - 667' 3,684 5,481 1,797 DRILL 12 1/4" INTERMEDIATE HOLE SECTION AS PER APROVED DIRECTIONAL PLAN # :00 23: ,684 5,093 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 3,684 ft TO 5,093 ft, 1,409 ft AT 78.3 FPH ROTATE DRILLED : 1,304 ft IN 14 HOUR AT 93.2 FPH AVERAGE ROP SLIDE DRILLED : 105 ft IN 4 HOUR AT FPH AVERAGE ROP 93% ROTATE, 7% SLIDE FULL RETURNS - MW :00 23: ,093 5,093 PERFORMED RIG / TOP DRIVE SERVICE INT DIR DRILL LUBRICATE RIG No 23:30 05: ,093 5,481 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 5,093 ft TO 5,481 ft, 388 ft AT 70.6 FPH ROTATE DRILLED : 356 ft IN 4.0 HOUR AT 89.0 FPH AVERAGE ROP SLIDE DRILLED : 32 ft IN 1.5 HOUR AT 21.3 FPH AVERAGE ROP 92% ROTATE, 8% SLIDE FULL RETURNS - MW 9.4+

11 Report End Date: 6/4/2016 Report Number: 13 Drilling Days: 4 : 5,822 : 341 Current VS (ft): 771 WASH AND REAM TO BOTTOM DRILL 12 1/4" INTERMEDIATE SECTION FROM 5,481 ft. TO 5,822 ft., MW 9.4 PPG., TOOH DUE TO LOW ROP, CHANGE BIT AND TIH TO 1,000 ft, WASH AND REAM F/1,000 ft T/ 2,200 ft LAST SURVEY: 5,682 ft. MD, 4.04 INC, 324 AZM. 7 BEHIND, 11 LEFT, BOTTOM HOLE TEMP 133 DISTANCE FROM : UNIVERSITY UNIT 1 RE HS - 569' UNIVERSITY UNIT 1 RE HA - 619' UNIVERSITY UNIT 1 RE HK - 704' 5,481 5, WASH AND REAM TO BOTTOM, DRILL 12 1/4" INTERMEDIATE HOLE SECTION AS PER APROVED DIRECTIONAL PLAN # :00 08: ,481 5,657 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 5,481 ft TO 5,657 ft, 176 ft AT 59 FPH ROTATE DRILLED : 176 ft IN 3 HOUR AT 59 FPH AVERAGE ROP SLIDE DRILLED : 0 ft IN 0 HOUR AT 0FPH AVERAGE ROP 100% ROTATE, 0% SLIDE FULL RETURNS - MW :00 08: ,657 5,657 REPAIR LEAK ON FLOW LINE INT DIR DRILL REPAIR RIG No 08:30 15: ,657 5,822 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 5,657 ft TO 5,822 ft, 165 ft AT 25 FPH ROTATE DRILLED : 145 ft IN 5 HOUR AT 29 FPH AVERAGE ROP SLIDE DRILLED : 20 ft IN 1.5 HOUR AT 13 FPH AVERAGE ROP 88% ROTATE, 12% SLIDE FULL RETURNS - MW :00 17: ,822 5,822 PUMP HIGH VIS LCM SWEEP MIXED AT 20 PPB AND CIRCULATE SURFACE TO SURFACE HOLE VOLUME WHILE ROTATE AND RECIPROCATE THE DRILL STRING WITH FULL RETURNS. 17:00 22: ,822 5,822 TOOH TO 3,000 ft IMPROPER HOLE FILL, WELL FLOWING AT 15 bph, SPOT 80 bbls OF 11.4 ppb PILL, FLOW CHECK WELL ( WELL STATIC )TOOH TO SURFACE, HOLE TAKING PROPER FILL 22:30 00: ,822 5,822 RACK BACK 12 1/4 in DIRECTIONAL BHA. CHANGE OUT 12 1/4 in PDC BIT. NOSE CUTTERS BROKE AND WORE INTO MATRIX OF BIT, 3/16 in OUT OF GAUGE. PICK UP HALLIBURTON MM65D, 9 X 18'S JETS, SN : INT DIR DRILL COND MUD & CIRC No INT DIR DRILL TRIPS No INT DIR DRILL P/U & L/D BHA No 00:30 01: ,822 5,822 TIH T/1,000 ft INT DIR DRILL TRIPS No 01:30 04: ,822 5,822 WASH IN HOLE F/1,000 ft T/2,200 ft AS NEEDED DUE TO BRIDGES AT 400 GPM WITH FULL RETURNS, MW 9.4 INT DIR DRILL REAMING No 04:30 05: ,822 5,822 PULL TRIP NIPPLE AND INSTALL ROTATING HEAD INT DIR DRILL BOP/OTHER No

12 Report End Date: 6/5/2016 Report Number: 16 Drilling Days: 5 : 6,155 : 333 Current VS (ft): 789 DRILLING 12 1/4" INTERMEDIATE HOLE SECTION WASH AND REAM F/2,200 ft T/ 5,822 ft, DRILL 12 1/4" INTERMEDIATE SECTION FROM 5,822 ft. TO 6,155 ft., CHANGE OUT ROTATING HEAD, BUILD 10 ppb LCM IN PITS AND START BY-PASSING SHAKERS, MW 9.4+ PPG LAST SURVEY: 6,058 ft. MD, 2.55 INC, 329 AZM. 3 AHEAD, 13 LEFT, BOTTOM HOLE TEMP 120 DISTANCE FROM : UNIVERSITY UNIT 1 RE HS - 582' UNIVERSITY UNIT 1 RE HA - 630' UNIVERSITY UNIT 1 RE HK - 726' 5,822 6, DRILL 12 1/4" INTERMEDIATE HOLE SECTION AS PER APROVED DIRECTIONAL PLAN # :00 14: ,822 5,822 WASH IN HOLE F/2,200 ft T/5/822 ft AS NEEDED DUE TO BRIDGES AT 500 GPM WITH FULL RETURNS, MW 9.4+ INT DIR DRILL REAMING No 14:30 15: ,822 5,845 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 5,822 ft TO 5,845 ft, 23 ft AT 46 FPH ROTATE DRILLED : 23 ft IN 0.5 HOUR AT 46 FPH AVERAGE ROP SLIDE DRILLED : 0 ft IN 0 HOUR AT 0 FPH AVERAGE ROP 100% ROTATE, 0% SLIDE FULL RETURNS - MW :00 15: ,845 5,845 PERFORMED RIG / TOP DRIVE SERVICE INT DIR DRILL LUBRICATE RIG No 15:30 18: ,845 5,951 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 5,845 ft TO 5,951 ft, 106 ft AT 42.4 FPH ROTATE DRILLED : 84 ft IN 1.0 HOUR AT 84 FPH AVERAGE ROP SLIDE DRILLED : 22 ft IN 1.5 HOUR AT 14.6 FPH AVERAGE ROP 79% ROTATE, 21% SLIDE FULL RETURNS - MW :00 19: ,951 5,951 CHANGE OUT ROTATING HEAD AND POSITION BOP STACK INT DIR DRILL 3rd PARTY EQUIPMENT REPAIR 19:30 21: ,951 6,033 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 5,951 ft TO 6,033 ft, 82 ft AT 54.6 FPH ROTATE DRILLED : 82 ft IN 1.5 HOUR AT 54.6 FPH AVERAGE ROP SLIDE DRILLED : 0 ft IN 0 HOUR AT 0 FPH AVERAGE ROP 100% ROTATE, 0% SLIDE FULL RETURNS - MW 9.4 Yes LOST PARTIAL RETURNS AT 6,033 ft PICK UP OFF BOTTOM, SLOW PUMPS TO 150 gpm AND BUILD 10 ppb LCM IN PITS ( LOST 20 bbls OBM ) 21:00 22: ,033 6,033 HOLE STARTED SEEPING MUD WHILE SLIDING AT 6,033 ft, BUILD 10 ppb LCM IN PITS AND START BY-PASSING SHAKERS 22:30 05: ,033 6,155 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 6,033 ft TO 6,155 ft, 122 ft AT 18.8 FPH ROTATE DRILLED : 84 ft IN 1.5 HOUR AT 56 FPH AVERAGE ROP SLIDE DRILLED : 38 ft IN 5.0 HOUR AT 7.6 FPH AVERAGE ROP 69% ROTATE, 31% SLIDE FULL RETURNS - MW 9.4+ INT DIR DRILL COND MUD & CIRC No CONTROL DRILL 80 FPH, 500 GPM MAINTAIN 10 PPB LCM MIXED AT 50/50 HULLS/CEDAR

13 Report End Date: 6/6/2016 Report Number: 15 Drilling Days: 6 : 7,226 : 1,071 Current VS (ft): 795 DRILLING 12 1/4" INTERMEDIATE HOLE SECTION DRILL 12 1/4" INTERMEDIATE SECTION FROM 6,155 ft. TO 7,226 ft. MAINTAIN 10 ppb LCM IN PITS MW 9.5 PPG LAST SURVEY: 7,094 ft. MD, 0.57 INC, 156 AZM. 8.8 AHEAD, 10.2 LEFT, BOTTOM HOLE TEMP 142 DISTANCE FROM : UNIVERSITY UNIT 1 RE HS - 742' UNIVERSITY UNIT 1 RE HA - 625' UNIVERSITY UNIT 1 RE HK - 718' 6,155 7,226 1,071 PERFORM CLEAN UP CYCLE, TOOH, LAY DOWN BHA, PULL WEAR BUSHING, RIH WITH 9 5/8 in INTERMEDIATE CSG AND CMT SAME, TEST CASING, SET AND TEST PACKOFF, SET WEAR BUSHING, PICK UP 8 3/4 in CURVE / LATERAL ASSY, TIH, DRILL OUT AND DRILL TO KOP AT 7,402 ft :00 05: ,155 7,226 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 6,155 ft TO 7,226 ft, 1,071 ft AT 44.6 FPH ROTATE DRILL: 1,009 ft IN 19.0 HOURS AT 53.1 FPH AVERAGE ROP SLIDE DRILL: 62 ft IN 5.0 HOUR AT 12.4 FPH AVERAGE ROP 94% ROTATE, 6% SLIDE FULL RETURNS - MW 9.5, BYPASSING SHAKERS WITH 10 PPB LCM IN SYSTEM, (50 % CEDAR FIBER / 50 % COTTON SEED)

14 Report End Date: 6/7/2016 Report Number: 16 Drilling Days: 7 : 7,300 : 74 Current VS (ft): 795 RIH WITH 9 5/8 in INTERMEDIATE CASING DRILL 12 1/4" INTERMEDIATE SECTION FROM 7226 ft. TO 7,300 ft. MAINTAIN 10 ppb LCM IN PITS MW 9.5 PPG. PERFORM CLEAN UP CYCLE, TOOH TO RUN INTERMEDIATE CASING, LAY DOWN DIRECTIONAL TOOLS, PULL WEAR BUSHING, RIG UP CASING CREW, RIH WITH 9 5/8 in INTERMEDIATE CASING T/2,800 ft CONTACTED AMY WITH TRRC OF UPCOMING 9 5/8 CEMENT JOB AT 15:00 hrs 6/6/16 *TD INTERMEDIATE SECTION 6/6/2016 AT 8:00 AM * LAST SURVEY: 7,231 ft. MD, 0.48 INC, 175 AZM. 8 AHEAD, 9 LEFT, BOTTOM HOLE TEMP 140 DISTANCE FROM : UNIVERSITY UNIT 1 RE HS - 559' UNIVERSITY UNIT 1 RE HA - 624' UNIVERSITY UNIT 1 RE HK - 717' 7,226 7, RIH WITH 9 5/8 in INTERMEDIATE CSG AND CMT SAME, TEST CASING TO 1500 psi, SET AND TEST PACKOFF, SET WEAR BUSHING, PICK UP 8 3/4 in CURVE / LATERAL ASSY, TIH, DRILL OUT AND DRILL TO KOP AT 7,425 ft :00 08: ,226 7,300 ROTATE / SLIDE DRILLED 12 1/4 in INTERMEDIATE HOLE FROM 7,226 ft TO 7,300 ft, 74 ft AT 24.6 FPH ROTATE DRILL: 74 ft IN HOURS AT 24.6 FPH AVERAGE ROP SLIDE DRILL: 0 ft IN 0 HOUR AT 0 FPH AVERAGE ROP 100% ROTATE, 0% SLIDE FULL RETURNS - MW 9.5, BYPASSING SHAKERS WITH 10 PPB LCM IN SYSTEM, (50 % CEDAR FIBER / 50 % COTTON SEED) *TD INTERMEDIATE SECTION 6/6/2016 AT 8:00 AM * 08:00 09: ,300 7,300 PERFORM CLEAN UP CYCLE AT 12.25in TD, PUMPED TWO HIGH VISC SWEEPS 30 MIN APART AND CIRCULATED SURFACE TO SURFACE HOLE VOLUME WHILE MAINTAIN 10 PPB LCM MIXED AT 50/50 HULLS/CEDAR, MW 9.5 PPG, CHECKED FLOW, WELL STATIC. 09:30 16: ,300 7,300 TOOH 5 STANDS, CHECKED FLOW, WELL STATIC, PUMPED SLUG,STRAP OUT HOLE TO RUN 9 5/8 in CASING INT DIR DRILL COND MUD & CIRC No INT DIR DRILL TRIPS No 16:30 17: ,300 7,300 PULL ROTATING HEAD AND INSTALL TRIP NIPPLE INT DIR DRILL BOP/OTHER No 17:00 19: ,300 7,300 LAID DOWN 12 1/4 in X 8 in DIRECTIONAL BHA INT DIR DRILL P/U & L/D BHA No 19:30 20: ,300 7,300 PULL WEAR BUSHING AND CLEAN RIG FLOOR INT DIR DRILL BOP/OTHER No 20:30 22: ,300 7,300 RIG UP PIPE PROS CASING RUNNING EQUIPMENT INT DIR CSG/CEMENT RUN CASING No 22:00 23: ,300 7,300 RUN INTERMEDIATE CASING TO 431 FT INT DIR CSG/CEMENT RUN CASING No 23:30 01: ,300 7,300 LAY DOWN 2 BAD JOINTS OF CASING, DUE TO TOP DRIVE OUT OF LINE INT DIR CSG/CEMENT REPAIR RIG Yes 01:30 05: ,300 7,300 RUN INTERMEDIATE CASING F/431 ft T/2,800 ft INT DIR CSG/CEMENT RUN CASING No

15 Report End Date: 6/8/2016 Report Number: 17 Drilling Days: 8 : 7,300 : 0 Current VS (ft): 795 PICK UP 8 3/4 CURVE/LATERAL ASSY RIH WITH 9 5/8 in INTERMEDIATE CASING TO 7,288 ft. RIG UP AND CIRCULATE 1 1/2 CASING VOLUMES & CEMENT SAME, TEST CASING T/1,500 PSI FOR 30 MINS, RIG DOWN CEMENT HEAD AND LANDING JOIN, WHILE CLEANING LCM FROM PITS. INSTALL PACKOFF AND TEST TO 3,000 PSI. PICK UP 8 3/4 CURVE/LATERAL ASSY LAST SURVEY: 7,231 ft. MD, 0.48 INC, 175 AZM. 8 AHEAD, 9 LEFT, BOTTOM HOLE TEMP 140 DISTANCE FROM : UNIVERSITY UNIT 1 RE HS - 559' UNIVERSITY UNIT 1 RE HA - 624' UNIVERSITY UNIT 1 RE HK - 717' 7,300 7,300 0 CONTINUE PICKING UP 8 3/4 CURVE/LATERAL BHA, LEVEL AND SHIM SUBS, DRILL OUT SHOE TRACK, DRILL TO KOP AT 7,425 ft AND DRILL CURVE AND LATERAL AS PER DIRECTIONAL PLAN #2 05:00 13: ,300 7,300 M/U SHOE TRACK AND CHECK LARKIN AUTO FILL FLOAT EQUIPMENT, RIH WITH 9 5/8 in CASING (187 JNTS + PUP JOINT + LANDING JOINT) in, 40 PPF,HCL-80/K-55, LTC, INTERMEDIATE CASING (DRIFTED TO 8.75 in). RAN CASING AT 60 ft/min. TAGGED BOTTOM, L/D TAG JT. AND LANDED CASING. W/ SHOE AT 7,288 ft. MAKE UP TORQUE: 5600 FT*LBS - K-55, 7270 FT*LBS - L-80. LARKIN AUTO-FILL FLOAT SHOE SET AT 7,288 ft. LARKIN AUTO-FILL FLOAT COLLAR AT 7,207 ft. DROP LARKIN 1 5/16 in BALL AT 6,800 ft TO GIVE TIME TO FALL WHILE RIH TO BTM INT DIR CSG/CEMENT RUN CASING No 13:30 18: ,300 7,300 INSTALL CEMENT HEAD, BREAK CIRCULATION, PUMP 50 BBLS OBM AT 3 BPM WITH 200 PSI, STAGE PUMPS TO 6 BPM WITH 400 PSI AND CONTINUE CIRCULATE 1 1/2 CASING VOLUME WITH FULL RETURNS, MAINTAINING MW 9.5, LCM 10 PPB NOTE: PRESSURE INCRESE 250 PSI WHEN 1 5/16 in BALL PASSED THROUGH FLOAT EQUIPMENT 18:00 23: ,300 7,300 PERFORMED CEMENT JOB AS FOLLOWS : TESTED LINES TO PSI. 50 BBLS 10.0 LB/GAL SPACER. PUMPED 587 BBLS * LEAD * ( 1250 SKS, 11.5 PPG,) OF 50/50 POZ C CMNT+ ADDITIVES AT 6 BPM, PUMPED 57 BBLS * TAIL * ( 200 SKS, 13.2 PPG ) OF C+ CEMENT + ADDITIVES AT 6 BPM, DISPLACED WITH 546 BBLS. OF 9.5 PPG OBM, SLOWED RATE TO 3 BPM WITH 30 BBLS REMAINING, BUMP PLUG, FINAL LIFT PRESSURE 750 PSI, BLED OFF PRESSURE AND FLOATS HELD, 50 BBLS OF CONTAMINATED CEMENT TO SURFACE, LOST RETURNS LAST 50 BBLS OF DISPLACEMENT ESTIMATED TOP OF LEAD CEMENT AT SURFACE, ESTIMATED TOP OF TAIL 6,371 ft, NOTIFIED "AMY" W/TXRRC AT 15:00 HRS ON 4/6/16 OF INTENT TO RUN AND CEMENT INTERMEDIATE CASING. INT DIR CSG/CEMENT COND MUD & CIRC No INT DIR CSG/CEMENT RUN CEMENT No 23:00 23: ,300 7,300 TEST 9 5/8 in CASING TO 1500 PSI AND HOLD FOR 30 MIN. TEST GOOD INT DIR CSG/CEMENT RUN CEMENT No 23:30 00: ,300 7,300 RIGGED DOWN CEMENT HEAD AND CIRCULATING IRON ( CLEANING LCM FROM PITS ) 00:00 00: ,300 7,300 REMOVED LANDING JOINT, RIGGED DOWN CASING ELEVATORS AND BALE EXTENSIONS. 00:30 02: ,300 7,300 RIH AND SET PACK OFF, POOH AND LAID DOWN SETTING TOOL, TESTED UPPER & LOWER SEALS TO 3,000 PSI ( TEST OK ). INT DIR CSG/CEMENT RUN CEMENT No INT DIR CSG/CEMENT RUN CEMENT No INT DIR CSG/CEMENT BOP/OTHER No 02:30 03: ,300 7,300 INSTALLED WEAR BUSHING INT DIR CSG/CEMENT BOP/OTHER No 03:00 03: ,300 7,300 CLEARED AND CLEANED RIG FLOOR INT DIR CSG/CEMENT TRIPS No 03:30 05: ,300 7,300 P/U 8 3/4 in MMD55DC PDC BIT, 6 3/4 in CATHEDRAL MUD MOTOR, 7/8 LOBE, 5.7 STAGE, FIXED 2.12 BEND, SLICK SLEEVE, BTB 5.64, CATHEDRAL EM TOOL INT DIR CSG/CEMENT P/U & L/D BHA No

16 Report End Date: 6/9/2016 Report Number: 18 Drilling Days: 9 : 7,818 : 518 Current VS (ft): 857 DRILLING 7,818 PICK UP 8 3/4 CURVE/LATERAL ASSY, AND SURFACE TEST SAME, TRIP IN HOLE, LEVEL RIG, DRILL OUT SHOE TRACK T/7,300 ft AND DRILL TO KOP AT 7,425 ft, DRILL CURVE FROM 7,425 ft TO 7,818 ft DRILL CURVE AND LATERAL AS PER DIRECTIONAL PLAN #2 7,425 ft MUD WT. 9.9 FULL RETURNS LAST SURVEY: 7,692 ft. MD, INC, AZM AHEAD, 11.2 LEFT, BOTTOM HOLE TEMP 142 MOTOR YIELD 11.0, DLN 7.8 DISTANCE FROM : UNIVERSITY UNIT 1 RE HS - 673' UNIVERSITY UNIT 1 RE HA - 651' UNIVERSITY UNIT 1 RE HK - 709' 7,300 7, :00 08: ,300 7,300 CONTINUE P/U 8 3/4 in MMD55DC PDC BIT, 6 3/4 in CATHEDRAL MUD MOTOR, 7/8 LOBE, 5.7 STAGE, FIXED 2.12 BEND, SLICK SLEEVE, BTB 5.64, CATHEDRAL EM TOOL, SURFACE TEST MWD AND MUD MOTOR NOTE: FLUSHED LCM FROM MUD PUMPS AND TOP DRIVE BEFORE SURFACE TEST INT DIR CSG/CEMENT DIRECTIONAL WORK No 08:00 12: ,300 7,300 T.I.H. WITH CURVE/LATERAL ASSEMBLY 7,205 ft INT DIR CSG/CEMENT TRIPS No 12:00 12: ,800 TRIP NIPPLE AND INSTALL ROTATING HEAD INT DIR CSG/CEMENT BOP/OTHER No 12:30 16: ,800 7,300 LEVEL RIG, PULLED MOUSE HOLE, INSTALL BEAMS FOR RAISING RIG, RAISE RIG AND LEVEL, INSTALL BOARDS UNDER SUBS 16:00 17: ,300 7,300 CHANGE OUT HYDRAULIC VALVE BODY FOR I-BOP AND LINK TILT ON TOP DRIVE WHILE INSTALLING MOUSE HOLE, CHANGE SHAKER SCREENS AND INSTALL TURN BUCKELS 17:30 18: ,300 7,300 DRILLED 9 5/8 in SHOE TRACK FROM 7,205 ft. TO 7,300 ft., TAG FLOAT AT 7,205 ft 18:30 21: ,300 7,425 ROTATE/SLIDE DRILLED FROM 7,300 ft TO 7,425 ft, 125 ft AT 50 FPH ROTATE DRILL: 125 ft IN 32.5 HOURS AT 50 FPH AVERAGE ROP SLIDE DRILL: 0 ft IN 0 HOURS AT 0 FPH AVERAGE ROP 100 % ROTATE, 0 % SLIDE FULL RETURNS, MW :00 05: ,425 7,818 ROTATE/SLIDE DRILLED FROM 7,425 ft TO 7,818 ft, 393 ft AT 49.1 FPH ROTATE DRILL: 70 ft IN 2.5 HOURS AT 28 FPH AVERAGE ROP SLIDE DRILL: 323 ft IN 5.5 HOURS AT 58.7 FPH AVERAGE ROP 18 % ROTATE, 82 % SLIDE FULL RETURNS, MW 9.9 INT DIR CSG/CEMENT REPAIR RIG Yes INT DIR CSG/CEMENT BOP/OTHER No INT DIR CSG/CEMENT DRILL W/ MUD No PROD DIR DRILL DRILL W/ MUD No PROD CURVE DRILL DRILL W/ MUD No

17 Report End Date: 6/10/2016 Report Number: 19 Drilling Days: 10 : 9,198 : 1,379 Current VS (ft): 2,036 DRILLING 9,198' DRILL CURVE FROM 7,819 ft TO 9,010 ft, DRILL LATERAL FROM 9,010 ft TO 9,198 ft 7,425 ft, LAND 9,010 ft MUD WT FULL RETURNS LAST SURVEY: 9,041 ft. MD, INC, 0.61 AZM. 3.5 AHEAD, 2.7 LEFT, BOTTOM HOLE TEMP 167 RECIEVED TAGET LINE CHANGE AT 14:00 AT 8,322 ft TL#3 8000', KBTVD AT 0' VS WITH INC, PLAN # 3, RECIEVED PLAN #4 FOR CORRECTION OLD LINE 7984', KBTVD AT INC AT 0 VS DRILL LATERAL AS PER DIRECTIONAL PLAN #4 7,819 9,198 1, :00 01: ,819 9,010 ROTATE/SLIDE DRILLED CURVE FROM 7,819 ft TO 9,010 ft, 1,191 ft AT FPH ROTATE DRILL: 800 ft IN 11.5 HOURS AT 69.6 FPH AVERAGE ROP SLIDE DRILL: 391 ft IN 8.5 HOURS AT 46.0 FPH AVERAGE ROP 67 % ROTATE, 33 % SLIDE FULL RETURNS, MW 10.7 PROD CURVE DRILL DRILL W/ MUD Yes 01:00 03: ,010 9,198 ROTATE/SLIDE DRILLED LATERAL FROM 9,010 ft TO 9,198 ft, 188 ft AT 75.2 FPH ROTATE DRILL: 176 ft IN 2.0 HOURS AT 88.0 FPH AVERAGE ROP SLIDE DRILL: 12 ft IN 0.5 HOURS AT 24.0 FPH AVERAGE ROP 94 % ROTATE, 6 % SLIDE FULL RETURNS, MW 10.7 PROD LAT DRILL DRILL W/ MUD No 03:30 05: ,198 9,198 TROUBLE SHOOT MWD PROD LAT DRILL 3rd PARTY EQUIPMENT REPAIR Yes

18 Report End Date: 6/11/2016 Report Number: 20 Drilling Days: 11 : 11,078 : 1,880 Current VS (ft): 3,973 DRILLING 11,078' DRILL LATERAL FROM 9,198 ft TO 11,078 ft DRILL LATERAL AS PER DIRECTIONAL PLAN #6 TARGET LINE #5 MUD WT FULL RETURNS LAST SURVEY: 10,921 ft. MD, 91.8 INC, 0.44 AZM., 1.8 ABOVE, 1.2 RIGHT, BOTTOM HOLE TEMP 178 RECIEVED TARGET LINE 2:00 am AT 10,795 ft TL#5, PLAN #6 7,954' KBTVD AT 0' VS WITH INC OLD TARGET LINE TL#4 7,964', KBTVD AT 0' VS WITH INC, 9,198 11,078 1, :00 13: ,198 9,856 ROTATE/SLIDE DRILLED LATERAL FROM 9,198 ft TO 9,856 ft, 658 ft AT 82.3 FPH ROTATE DRILL: 612 ft IN 6.5 HOURS AT 94.2 FPH AVERAGE ROP SLIDE DRILL: 46 ft IN 1.5 HOURS AT 30.7 FPH AVERAGE ROP 93 % ROTATE, 7 % SLIDE FULL RETURNS, MW 10.7 PROD LAT DRILL DRILL W/ MUD No 13:00 14: ,856 9,856 RE-LOG GAMMA PROD LAT DRILL 3rd PARTY EQUIPMENT REPAIR 14:00 15: ,856 9,949 ROTATE/SLIDE DRILLED LATERAL FROM 9,856 ft TO 9,949 ft, 93 ft AT 62.0 FPH ROTATE DRILL: 93 ft IN 1.5 HOURS AT 62.0 FPH AVERAGE ROP SLIDE DRILL: 0 ft IN 0 HOURS AT 0 FPH AVERAGE ROP 100 % ROTATE, 0 % SLIDE FULL RETURNS, MW 10.7 PROD LAT DRILL DRILL W/ MUD No 15:30 16: ,949 9,949 RE-LOG GAMMA PROD LAT DRILL 3rd PARTY EQUIPMENT REPAIR 16:00 17: ,949 10,043 ROTATE/SLIDE DRILLED LATERAL FROM 9,949 ft TO 10,043 ft, 94 ft AT 62.7 FPH ROTATE DRILL: 84 ft IN 1.0 HOURS AT 84.0 FPH AVERAGE ROP SLIDE DRILL: 10 ft IN 0.5 HOURS AT 20.0 FPH AVERAGE ROP 89 % ROTATE, 11 % SLIDE FULL RETURNS, MW 10.7 PROD LAT DRILL DRILL W/ MUD No 17:30 18: ,043 10,043 RE-LOG GAMMA PROD LAT DRILL 3rd PARTY EQUIPMENT REPAIR 18:00 23: ,043 10,513 ROTATE/SLIDE DRILLED LATERAL FROM 10,043 ft TO 10,513 ft, 470 ft AT 94.0 FPH ROTATE DRILL: 435 ft IN 4.0 HOURS AT FPH AVERAGE ROP SLIDE DRILL: 35 ft IN 1.0 HOURS AT 35.0 FPH AVERAGE ROP 93 % ROTATE, 7 % SLIDE FULL RETURNS, MW 10.7 PROD LAT DRILL DRILL W/ MUD No 23:00 23: ,513 10,513 PERFORMED RIG / TOP DRIVE SERVICE PROD LAT DRILL LUBRICATE RIG No 23:30 05: ,513 11,078 ROTATE/SLIDE DRILLED LATERAL FROM 10,513 ft TO 11,078 ft, 565 ft AT FPH ROTATE DRILL: 545 ft IN 5.0 HOURS AT FPH AVERAGE ROP SLIDE DRILL: 20 ft IN 0.5 HOURS AT 40.0 FPH AVERAGE ROP 96 % ROTATE, 4 % SLIDE FULL RETURNS, MW 10.7 RECIEVED TARGET LINE 2:00 am AT 10,795 ft, TL#5, PLAN #6 7954' KBTVD AT 0' VS WITH INC PROD LAT DRILL DRILL W/ MUD No Yes Yes Yes

19 Report End Date: 6/12/2016 Report Number: 21 Drilling Days: 12 : 7,965 : 476 Current VS (ft): 1,023 TIME DRILLING 5/MINS INCH AT 7,965 ft F/SIDETRACK DRILL LATERAL FROM 11,078 ft TO 11,549 ft AT 11,549, CIRCULATED 3 BOTTOMS UP PREPARED TO TRIP OUT TO 7,960 ft TO SIDE TRACK WELL, TROUGH WELLBORE AND BEGIN TIME DRILLING F/7,960 ft T/7,965 ft AT 5 MINS INCH MUD WT FULL RETURNS LAST SURVEY: 11,486 ft. MD, INC, 3.34 AZM., 4.6 ABOVE, 2.1 LEFT, BOTTOM HOLE TEMP 180 RECIEVED TARGET LINE 10:30 am AT 11,549 ft, ST01 TL#1, PLAN #7 7,984' KBTVD AT 0' VS WITH INC OLD TARGET LINE TL#5, PLAN #6 7,954' KBTVD AT 0' VS WITH INC 11,078 7, SIDE TRACK, TIME DRILL T/8,000 ft AND CONTINUE DRILLING CURVE AS PER ST01, TL #1, PLAN # :00 10: ,078 11,549 ROTATE/SLIDE DRILLED LATERAL FROM 11,078 ft TO 11,549 ft, 471 ft AT 85.6 FPH ROTATE DRILL: 431 ft IN 4.0 HOURS AT FPH AVERAGE ROP SLIDE DRILL: 40 ft IN 1.5 HOURS AT 26.7 FPH AVERAGE ROP 92 % ROTATE, 8 % SLIDE FULL RETURNS, MW 10.7 PROD LAT DRILL DRILL W/ MUD No RECIEVED TARGET LINE 10:30 am AT 11,549 ft, ST01 TL#1, PLAN #7 7,984' KBTVD AT 0' VS WITH INC 10:30 13: ,960 7,960 CIRCULATE HI-VIS SWEEP PROD CURVE DRILL COND MUD & CIRC Yes 13:30 17: ,960 7,960 CHECKED FLOW, WELL STATIC, PUMPED SLUG, TOOH FROM 11,549 ft TO 7,960 ft, COUNT PIPE IN HOLE, DERRICK AND ON THE PIPE RACKS BEFORE STARTING GEOLOGICAL SIDETRACK PROD CURVE DRILL TRIPS Yes 17:30 23: ,960 7,960 TROUGHING F/7,915 ft T/7,960 ft PROD CURVE DRILL DIRECTIONAL WORK Yes 23:00 05: ,960 7,965 SLIDE/TIME DRILL F/7,960 ft T/7,965 ft AT 5 MINUTES AN INCH FOR 5 ft PROD CURVE DRILL DRILL W/ MUD Yes

20 Report End Date: 6/13/2016 Report Number: 22 Drilling Days: 13 : 8,132 : 167 Current VS (ft): 1,068 DRILLING 8,132 ft TIME DRILLING F/7,965 ft T/7,975 ft AT 5 MINS INCH, F/7975 ft T/7980 AT 4 MINS INCH, F/7,980 ft T/7,985 ft AT 3 MINS INCH, F/7,985 ft T/7,990 ft AT 2 MINS INCH, 7,990 ft T/8,000 ft AT 1 MIN INCH, SLIDE DRILL CURVE F/8,000 ft T/8,132 ft DRILL CURVE AND LATERAL AS PER DIRECTIONAL PLAN ST01, TL #1, PLAN #7 MUD WT FULL RETURNS LAST SURVEY: 8,038 ft. MD, INC, 9.05 AZM., 1.6 BEHIND, 3.8 RIGHT, BOTTOM HOLE TEMP 167 DISTANCE FORM OLD WELLBORE 16.6 ft TARGET LINE ST01 TL#1, PLAN #7 7,984' KBTVD AT 0' VS WITH INC OLD TARGET LINE TL#5, PLAN #6 7,954' KBTVD AT 0' VS WITH INC 7,965 8, :00 00: ,965 8,000 SLIDE/TIME DRILL F/7,965 ft T/7,975 ft AT 5 MINS INCH, F/7975 ft T/7980 AT 4 MINS INCH, F/7,980 ft T/7,985 ft AT 3 MINS INCH, F/7,985 ft T/7,990 ft AT 2 MINS INCH, 7,990 ft T/8,000 ft AT 1 MIN INCH ROTATE DRILL: 0 ft IN 0 HOURS AT 0 FPH AVERAGE ROP SLIDE DRILL: 35 ft IN 19 HOURS AT 1.8 FPH AVERAGE ROP 0 % ROTATE, 100 % SLIDE FULL RETURNS, MW 10.7 PROD CURVE DRILL DRILL W/ MUD Yes 00:00 05: ,000 8,132 ROTATE/SLIDE DRILLED CURVE FROM 8,000 ft TO 8,132 ft, 132 ft AT 26.4 FPH ROTATE DRILL: 0 ft IN 0.0 HOURS AT 0 FPH AVERAGE ROP SLIDE DRILL: 132 ft IN 5.0 HOURS AT 26.4 FPH AVERAGE ROP 0 % ROTATE, 100 % SLIDE FULL RETURNS, MW 10.7 PROD CURVE DRILL DRILL W/ MUD Yes

21 Report End Date: 6/14/2016 Report Number: 23 Drilling Days: 14 : 9,856 : 1,725 Current VS (ft): 2,678 DRILLING LATERAL AT 9,856 ft DRILL CURVE F/8,132 ft T/8,539 ft DRILLING LATERAL F/ 8,539 ft - 9,856 ft LANDED CURVE AT 8,539 AT 13:30 6/13/16 DRILL LATERAL AS PER DIRECTIONAL PLAN ST01, TL #1, PLAN #7 MUD WT FULL RETURNS LAST SURVEY: 9,699 ft. MD, INC, 6.59 AZM., 3.3 BELOW, 9.0 LEFT, BOTTOM HOLE TEMP 178 DISTANCE FORM OLD WELLBORE 136 ft TARGET LINE ST01 TL#1, PLAN #7 7,984' KBTVD AT 0' VS WITH INC 8,132 9,856 1, :00 13: ,132 8,539 ROTATE/SLIDE DRILLED CURVE FROM 8,132 ft TO 8,539 ft, 407 ft AT 45.2 FPH ROTATE DRILL: 243 ft IN 4.75 HOURS AT 51.2 FPH AVERAGE ROP SLIDE DRILL: 164 ft IN 4.25 HOURS AT 38.6 FPH AVERAGE ROP 60 % ROTATE, 40 % SLIDE FULL RETURNS, MW 10.7 PROD CURVE DRILL DRILL W/ MUD Yes 13:30 22: ,539 9,386 ROTATE/SLIDE DRILLED LATERAL FROM 8,539 ft TO 9,386 ft, 847 ft AT 99.7 FPH ROTATE DRILL: 816 ft IN 6.75 HOURS AT FPH AVERAGE ROP SLIDE DRILL: 31 ft IN 1.75 HOURS AT 17.7 FPH AVERAGE ROP 96 % ROTATE, 4 % SLIDE FULL RETURNS, MW 10.8 PROD LAT DRILL DRILL W/ MUD Yes 22:30 23: ,386 9,386 PERFORMED RIG / TOP DRIVE SERVICE PROD LAT DRILL LUBRICATE RIG Yes 23:00 05: ,386 9,856 ROTATE/SLIDE DRILLED LATERAL FROM 9,386 ft TO 9,856 ft, 470 ft AT 78.3 FPH ROTATE DRILL: 438 ft IN 4.0 HOURS AT FPH AVERAGE ROP SLIDE DRILL: 32 ft IN 2.0 HOURS AT 16.0 FPH AVERAGE ROP 93 % ROTATE, 7 % SLIDE FULL RETURNS, MW 10.8 PROD LAT DRILL DRILL W/ MUD Yes

22 Report End Date: 6/15/2016 Report Number: 24 Drilling Days: 15 : 11,737 : 1,881 Current VS (ft): 4,711 DRILLING LATERAL AT 11,737 ft DRILLED LATERAL F/ 9,856 ft - 10,795 ft, PERFORMED RIG / TOP DRIVE SERVICE, CONT, DRILLING LATERAL TO 11,737 ft. DRILL LATERAL AS PER DIRECTIONAL PLAN ST01, TL #1, PLAN #7 MUD WT FULL RETURNS LAST SURVEY: 11,580 ft. MD, INC, AZM., 4.6 ABOVE, 5.1 RIGHT, BOTTOM HOLE TEMP IS 185 DISTANCE FORM OLD WELLBORE 148 ft TARGET LINE ST01 TL#1, PLAN #7 7,984' KBTVD AT 0' VS WITH INC 9,856 11,737 1, :00 16: ,856 10,795 ROTATE/SLIDE DRILLED LATERAL FROM 9,856 ft TO 10,795 ft, 939 ft AT 81.6 FPH ROTATE DRILL: 859 ft IN 7.0 HOURS AT FPH AVERAGE ROP SLIDE DRILL: 80 ft IN 4.5 HOURS AT 17.8 FPH AVERAGE ROP 91 % ROTATE, 9 % SLIDE, FULL RETURNS, MW 10.8 PROD LAT DRILL DRILL W/ MUD Yes 16:30 17: ,795 10,795 PERFORMED RIG / TOP DRIVE SERVICE PROD LAT DRILL LUBRICATE RIG Yes 17:00 02: ,795 11,549 ROTATE/SLIDE DRILLED LATERAL FROM 10,795 ft TO 11,549 ft, 754 ft AT 77.3 FPH ROTATE DRILLED 730 ft IN 8.25 HOURS AT 88.5 FPH AVERAGE ROP, SLIDE DRILLED: 24 ft IN 1.5 HOURS AT 16.0 FPH AVERAGE ROP 97 % ROTATE, 3 % SLIDE, FULL RETURNS, MW :45 05: ,549 11,737 ROTATE/SLIDE DRILLED LATERAL FROM 11,549 ft TO 11,737 ft, 188 ft AT FPH ROTATE DRILL: 188 ft IN 2.25 HOURS AT FPH AVERAGE ROP SLIDE DRILL: 0 ft IN 0 HOURS AT 0 FPH AVERAGE ROP 100 % ROTATE, 0 % SLIDE, FULL RETURNS, MW 10.8 PROD LAT DRILL DRILL W/ MUD Yes PROD LAT DRILL DRILL W/ MUD No

23 Report End Date: 6/16/2016 Report Number: 25 Drilling Days: 16 : 13,067 : 1,330 Current VS (ft): 6,040 CHANGING OUT BELT ON # 2 ENGINE DRILLED LATERAL F/ 11,737 ft - 12,771 ft, PERFORMED RIG / TOP DRIVE SERVICE, CONT. DRILLING LATERAL TO 13,067 ft., CIRCULATED AND CHANGED OUT BELT ON # 2 ENGINE DRILL LATERAL AS PER DIRECTIONAL PLAN ST01, TL #1, PLAN #7 MUD WT FULL RETURNS LAST SURVEY: 12,990 ft. MD, 90.4 INC, AZM., 9.2 ft. ABOVE, 10.3 ft. LEFT, BOTTOM HOLE TEMP WAS PAST VERTICAL SECTION OF PREVIOUS WELLBORE TARGET LINE ST01 TL#1, PLAN #7 7,984' KBTVD AT 0' VS WITH INC 11,737 13,067 1, :00 22: ,737 12,771 ROTATE/SLIDE DRILLED LATERAL FROM 11,737 ft TO 12,771 ft, 1,034 ft AT FPH ROTATE DRILLED: 997 ft IN 14.5 HOURS AT FPH AVERAGE ROP, SLIDE DRILLED: 37 ft IN 2.5 HOURS AT 14.8 FPH AVERAGE ROP, % ROTATE, 3.58 % SLIDE, FULL RETURNS, MW 10.8 PROD LAT DRILL DRILL W/ MUD No 22:00 22: ,771 12,771 PERFORMED RIG / TOP DRIVE SERVICE PROD LAT DRILL LUBRICATE RIG No 22:30 03: ,771 13,067 ROTATE/SLIDE DRILLED LATERAL FROM 12,771 ft TO 13,0671 ft, 296 ft AT 59.2 FPH ROTATE DRILLED: 273 ft IN 3.5 HOURS AT 78.0 FPH AVERAGE ROP, SLIDE DRILLED: 23 ft IN 1.5 HOURS AT 15.3 FPH AVERAGE ROP, % ROTATE, 7.78 % SLIDE, FULL RETURNS, MW :30 05: ,067 13,067 CIRCULATED AT REDUCED RATE ( 419 GPM ) WHILE REPLACING BELT ON # 2 ENGINE PROD LAT DRILL DRILL W/ MUD No PROD LAT DRILL REPAIR RIG Yes

24 Report End Date: 6/18/2016 Report Number: 27 Drilling Days: 18 : 14,135 : 0 Current VS (ft): 7,107 T.I.H. T.O.O.H. AND LAYED DOWN BHA #4 ; PICKED UP BHA #5, T.I.H. TO 7,223 ft., SLIPPED AND CUT DRLNG. LINE, PERFORMED RIG / TOP DRIVE SERVICE, CONTINUED T.I.H. TO 7,915 ft., ORIENTED DRILLING ASSY.,CONTINUED T.I.H. TO 8,740 ft., RETRIEVED TRIP NIPPLE AND ISTALLED R/HEAD RUBBER,T.I.H. TO 13,000 ft. MUD WT WITH FULL RETURNS LAST SURVEY: 14,025 ft. MD, INC, AZM.,.7 ft. ABOVE, 6.1 ft. RIGHT, BOTTOM HOLE TEMP WAS PAST VERTICAL SECTION OF PREVIOUS WELLBORE FINISH TRIP, DRILL LATERAL AS PER APPROVED DIRECTIONAL PLAN ST01, TL # 2, PLAN # 8 14,135 14, :00 07: ,135 14,135 CONTINUED T.O.O.H. TO 7,046 ft. ( NO ABNORAL DRAG ENCOUNTERED AND HOLE TOOK PROPER FILL ) PROD LAT DRILL TRIPS No 07:30 08: ,135 14,135 RETRIEVED ROTATING HEAD RUBBER AND INSTALLED TRIP NIPPLE PROD LAT DRILL BOP/OTHER No 08:00 12: ,135 14,135 CONTINUED T.O.O.H. TO 175 ft. PROD LAT DRILL TRIPS No 12:00 13: ,135 14,135 DRAINED MUD MOTOR, BROKE BIT OFF,LAYED DOWN MUD MOTOR AND SHOCK SUB PROD LAT DRILL P/U & L/D BHA No 13:00 13: ,135 14,135 CLEARED AND CLEANED RIG FLOOR PROD LAT DRILL TRIPS No 13:30 16: ,135 14,135 CHANGED OUT BATTERIES IN EM TOOL ; MADE UP MUD MOTOR AND BIT ; TESTED SAME ( TESTED GOOD ) PROD LAT DRILL P/U & L/D BHA No 16:00 20: ,135 14,135 P/U NEW SHOCK SUB ; T.I.H. FROM 175 ft. TO 7,223 ft. PROD LAT DRILL TRIPS No 20:00 23: ,135 14,135 SLIPPED AND CUT 14 WRAPS OF DRILLING LINE WHILE MONITORING WELL ON TRIP TANK ( WELL STATIC - NO GAINS OR LOSSES ) PROD LAT DRILL CUT SLIP & DRILL LINE No 23:00 23: ,135 14,135 PERFORMED RIG / TOP DRIVE SERVICE PROD LAT DRILL LUBRICATE RIG No 23:30 02: ,135 14,135 T.I.H. TO 7,915 ft., ORIENTED DRILLING ASSY.,T.I.H. TO 7,985 ft., PUMPED UP SURVEY TO COMPARE WITH ACTUAL SURVEY AT THAT DEPTH, ( OK ), CONTINUED T.I.H. TO 8,740 ft. PROD LAT DRILL TRIPS No 02:00 02: ,135 14,135 RETRIEVED TRIP NIPPLE AND INSTALLED ROTATING HEAD RUBBER PROD LAT DRILL BOP/OTHER No 02:30 05: ,135 1,435 T.I.H. FROM 8,740 ft.to 13,000 ft. PROD LAT DRILL TRIPS No

25 Report End Date: 6/19/2016 Report Number: 28 Drilling Days: 19 : 15,702 : 1,567 Current VS (ft): 8,671 Total Depth Date 6/19/2016 PERFORMING CLEAN-UP CYCLE AT T.D. Rig Release Date T.I.H. TO 14,135 ft. WASHING THE LAST STAND TO BOTTOM,DRILLED LATERAL F/ 14,135 ft 15,403 ft,performed RIG / TOP DRIVE SERVICE, CONT. DRILLING LATERAL TO T.D. AT 15,702 ft., PERFORMED CLEAN-UP CYCLE MUD WT ppg. WITH FULL RETURNS LAST SURVEY: 15,623 ft. MD, INC, 2.81 AZM., 6.8 ft. ABOVE, 12.6 ft. RIGHT, BOTTOM HOLE TEMP WAS 185 PAST VERTICAL SECTION OF PREVIOUS WELLBORE TARGET LINE CHANGE RECEIVED AT 18:00 ( ,053 ft. ) NEW TARGET LINE ST01 -TL # 3, PLAN # ' KBTVD AT 0 VS WITH INC OLD TARGET LINE ST01 - TL # 2, PLAN # ' KBTVD AT 0' VS WITH 90.3 INC PTB AT TD ( 15,702 ft. ) INC, 2.81 AZM., 6.8 ft. ABOVE AND 16 ft. RIGHT 14,135 15,702 1,567 Target Formation PERFORM CLEAN-UP CYCLE,CHECK FLOW,T.O.O.H. WITH 10 STDS. OF DRILLPIPE,CHECK FLOW,PUMP SLUG,T.O.O.H. TO RUN PRODUCTION CASING, ( SLM ) L/D B.H.A,RETRIEVE WEAR BUSHING, R/U AND RUN CASING :00 06: ,135 14,135 T.I.H. ; WASHED LAST STAND TO 14,135 ft. PROD LAT DRILL TRIPS No 06:00 22: ,135 15,403 ROTATE/SLIDE DRILLED LATERAL FROM 14,135 ft TO 15,403 ft, 1,268 ft AT FPH, ROTATE DRILLED: 1,172 ft IN 11 HOURS AT FPH AVERAGE ROP, SLIDE DRILLED: 96 ft IN 5.5 HOURS AT FPH AVERAGE ROP, % ROTATE, 7.57 % SLIDE, FULL RETURNS, MW 10.9 PROD LAT DRILL DRILL W/ MUD No 22:30 23: ,403 15,403 PERFORMED RIG / TOP DRIVE SERVICE PROD LAT DRILL LUBRICATE RIG No 23:00 04: ,403 15,702 ROTATE/SLIDE DRILLED LATERAL FROM 15,403 ft TO 15,702 ft, 299 ft AT 59.8 FPH, ROTATE DRILLED: 275 ft IN 3.5 HOURS AT FPH AVERAGE ROP, SLIDE DRILLED: 24 ft IN 1.5 HOURS AT 16 FPH AVERAGE ROP, 92 % ROTATE, 8 % SLIDE, FULL RETURNS, MW 10.9 PROD LAT DRILL DRILL W/ MUD No 04:00 05: ,702 15,702 CHECKED FLOW ( WELL STATIC ) ; PERFORMED CLEAN-UP CYCLE PROD LAT DRILL COND MUD & CIRC No

26 Report End Date: 6/20/2016 Report Number: 29 Drilling Days: 20 : 15,702 : 0 Current VS (ft): 8,671 T.O.O.H. Total Depth Date 6/19/2016 Rig Release Date PERFORMED CLEAN-UP CYCLE, PUMPED OUT OF HOLE FROM 15,702 ft. TO 15,240 ft., T.O.O.H. ( WET ) FROM 15,240 ft. TO 14,761 ft., PUMPED SLUG, T.O.O.H.CHECKED FLOW AT EOC, WORKED THROUGH SIDE TRACK, TOOK SURVEY AT 8,047 ft. ( OK ), PERFORMED RIG / TOP DRIVE SERVICE, CONT. T.O.O.H. TO 4,842 ft., C/O VERSA VALVE ON DRAWWORKS BRAKES, T.O.O.H. TO 700 ft. MUD WT ppg. NOTE : B.O.P. TEST DUE TOMORROW Target Formation FINISH T.O.O.H. ( SLM ) ; L/D B.H.A,RETRIEVE WEAR BUSHING, R/U AND RUN 5 1/2" PRODUCTION CASING AS PER APPROVED CASING TALLY NOTE : B.O.P. TEST DUE TOMORROW LAST SURVEY: 15,623 ft. MD, INC, 2.81 AZM., 6.8 ft. ABOVE, 12.6 ft. RIGHT, BOTTOM HOLE TEMP WAS 185 PTB AT TD ( 15,702 ft. ) INC, 2.81 AZM., 6.8 ft. ABOVE AND 16 ft. RIGHT 15,702 15, :00 16: ,702 15,702 PERFORMED CLEAN UP CYCLE : TOP DRIVE AT 70 RPM, 535 GPM. PUMPED (40bbl HI-VIS/LCM ) TANDEM SWEEPS 30 MIN APART: 1ST SWEEP : 100% SHAKER SCREEN COVERAGE : STARTING TORQUE 10,000, ENDING 10,000 2ND SWEEP : 100 %SHAKER SCREEN COVERAGE : STARTING TORQUE 10,000, ENDING 9,000 3RD SWEEP: 80% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9,000. 4TH SWEEP: 80% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9,000. 5TH SWEEP: 70% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9,000 6TH SWEEP: 70% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9,000. 7TH SWEEP: 60% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9,000. 8TH SWEEP: 60% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9,000. 9TH SWEEP: 60% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9, TH SWEEP: 50% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9,000. : PUMPED 2 (40 bbl HI-VIS/LCM/WEIGHTED ( 11.9 PPG ) TANDEM SWEEPS 30 MIN APART: 11TH SWEEP: 35% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9, TH SWEEP: 35% SHAKER SCREEN COVERAGE; STARTING TQ 9,000, ENDING TQ 9,000. CHECKED FLOW ( WELL STATIC ) PROD LAT DRILL COND MUD & CIRC No 16:00 23: ,702 15,702 PUMPED OUT OF HOLE FROM 15,702 ft. TO 15,240 ft., PULLED 5 STANDS WET WITHOUT PUMPING TO 14,761 ft.,pumped SLUG AND T.O.O.H. TO 8,539 ft., CHECKED FLOW ( WELL STATIC ), CONT. T.O.O.H. TO 7,960 ft. AND WORKED THROUGH SIDE TRACK WITH NO PROBLEM, T.O.O.H. TO 7,200 ft.,took SURVEY AT 8,047 ft. ( OK ), NO ABNORMAL DRAG ENCOUNTERED AND HOLE TOOK PROPER FILL PROD LAT DRILL TRIPS No 23:30 00: ,702 15,702 PERFORMED RIG / TOP DRIVE SERVICE PROD LAT DRILL LUBRICATE RIG No 00:00 01: ,702 15,702 T.O.O.H. FROM 7,200 ft. TO 4,842 ft. PROD LAT DRILL TRIPS No 01:30 02: ,702 15,702 REPLACED VERSA VALVE ON DRAW WORKS BRAKES ( VALVE WAS NOT DUMPING ) AND WOULD NOT ALLOW 'PARK " MODE WITHOUT A SIGNIFICANT DELAY PROD LAT DRILL REPAIR RIG Yes 02:00 05: ,702 15,702 CONTINUED T.O.O.H. FROM 4,842 ft. TO 700 FT. PROD LAT DRILL TRIPS No

27 Report End Date: 6/21/2016 Report Number: 30 Drilling Days: 21 : 15,702 : 0 Current VS (ft): 8,671 CIRCULATING Total Depth Date 6/19/2016 Rig Release Date TRIPPED OUT, LAYED DOWN DIRECTIONAL TOOLS, PULLED WEAR BUSHING, CLEANED FLOOR,HPJSM WITH CASING CREW AND RIGGED UP CASING CREW, RAN CASING TO BOTTOM AT 15,702 ft., L/O TAG JT., P/U PUP JT.,R/D " PIPE PROS " CSNG. TOOLS, R/U "NINE" CEMENTERS, RUPTURED TCO PLUG, PERCOLATED AIR OUT OF CASING MUD WT ppg. Target Formation CIRCULATE 2 BOTTOMS UP, PERFORM CEMENT JOB, R/D CEMENTERS,W.O.C. FOR 12 HRS.,INSTALL CSNG. SLIPS.,RELEASE RIG TO UNIVERSITY UNIT 1 RE HK, PREP FOR SKIDDING OPERATIONS CONTACTED TAMMY WITH THE RRC ON 6/19/16 AT 07:20 LAST SURVEY: 15,623 ft. MD, INC, 2.81 AZM., 6.8 ft. ABOVE, 12.6 ft. RIGHT, BOTTOM HOLE TEMP WAS 185 PTB AT TD ( 15,702 ft. ) INC, 2.81 AZM., 6.8 ft. ABOVE AND 16 ft. RIGHT 15,702 15, :00 06: ,702 15,702 T.O.O.H. TO 175 ft. PROD LAT DRILL TRIPS No 06:30 08: ,702 15,702 DRAINED MUD MOTOR ; BROKE BIT OFF AND L/D DIRECTIONAL TOOLS PROD LAT DRILL P/U & L/D BHA No 08:30 09: ,702 15,702 RETRIEVED WEAR BUSHING ; CLEARED AND CLEANED RIG FLOOR PROD LAT DRILL BOP/OTHER No 09:30 10: ,702 15,702 PJSM WITH " PIPE PROS " CASING CREW ; R/U CASING TOOL PROD PROD CSG/CEMENT RUN CASING No 10:30 03: ,702 15,702 PJSM WITH " PIPE PROS " CASING CREW, TRICAN TECH AND RIG CREW ; RAN PRODUCTION CASING AS PER APPROVED CASING TALLY TO 15,702 ft., TAGGED BOTTOM, L/O TAG JOINT AND P/U 1 PUP JT. LEAVING CASING SHOE AT 15,695 ft. RAN A TOTAL OF 347 JOINTS, 1 PUP JOINT AND 3 " MARKER JOINTS OF 5.5" - 17# HCP-110 LTC PRODUCTION CASING WITH FULL RETURNS - FLOTATION COLLAR AT 7,426.4 ft., FLOAT COLLAR AT 15, ft. NOTE : NOTIFIED "TAMMY" W/TXRRC AT 07:20 HRS ON 6/20/16 OF INTENT TO RUN AND CEMENT THIS PRODUCTION CASING STRING. 03:00 04: ,702 15,702 R/D CASING CREW ; R/U " NINE " CEMENT HEAD AND IRON, FILLED CASING. 04:00 05: ,702 15,702 RUPTURED FLOTATION TCO PLUG AT 1,820 PSI WITH RIG PUMP; LET MUD FREE FALL FOR 20 MINUTES AND PERCOLATED AIR OUT OF CASING PROD PROD CSG/CEMENT RUN CASING No PROD PROD CSG/CEMENT RUN CASING No PROD PROD CSG/CEMENT COND MUD & CIRC No

28 Report End Date: 6/22/2016 Report Number: 31 Drilling Days: 22 : 15,702 : 0 Current VS (ft): 8,671 INSTALLING CASING SLIPS Total Depth Date 6/19/2016 Rig Release Date CEMENTED PRODUCTION CASING AS PER APPROVED CMNT.PROGRAM, WOC FOR 12 HOURS, FLUSHED STACK, BROKE AND RAISED SAME, INSTALLED CASING SLIPS WITH 155K MUD WT ppg. Target Formation MAKE ROUGH CUT ON CASING AT 10in's WITH SWECO TECH, LAY DOWN CUT JOINT. MAKE FINAL CUT ON CASING AT 6in.'s, INSTALL TA CAP AND TORQUE UP SAME.RELEASE RIG TO UNIVERSITY UNIT 1 RE HK, PREP FOR SKIDDING OPERATIONS LAST SURVEY: 15,623 ft. MD, INC, 2.81 AZM., 6.8 ft. ABOVE, 12.6 ft. RIGHT, BOTTOM HOLE TEMP WAS 185 PTB AT TD ( 15,702 ft. ) INC, 2.81 AZM., 6.8 ft. ABOVE AND 16 ft. RIGHT 15,702 15, :00 10: ,702 15,702 COMPLETED CIRCULATING 2 BTMS UP VOLUMES AT 7 bpm WITH FULL RETURNS. - HELD PJSM WITH CEMENTERS, TRICAN FIELD REP AND RIG CREW. PROD PROD CSG/CEMENT COND MUD & CIRC No 10:00 15: ,702 15,702 R/U NINE CEMENTERS, TESTED LINES TO 8,000 PSI, PUMPED 100 BBL 11.4 ppg SPACER W/20 LB/BBL KOL SEAL, PUMPED 310 BBLS * LEAD * + ADDITIVES (1220 SKS, 13.5 ppg, 1.43 YIELD) AT 6 BPM, PUMPED 519 BBLS * TAIL * + ADDITIVES (2275 SKS, 14.4 ppg, YIELD 1.28) AT 6 BPM. DROPPED TRICAN 5 1/2 in 12 FIN WIPER DART (TOP PLUG), DISPLACED WITH 50 BBLS. OF 8.4 PPG SUGAR WATER FOLLOWED WITH 314 BBLS OF 8.4 PPG TREATED WATER, CAUGHT CEMENT 50 BBLS INTO DISPLACEMENT, PLUG BUMPED AS CALCULATED. FINAL PUMP PRESSURE 1920 psi, BUMPED TO 2,900 psi. LOST RETURNS 65 BBLS INTO DISPLACEMENT. NO CEMENT TO SURFACE; ESTIMATED TOP OF LEAD ft, ESTIMATED TOP OF TAIL AT 4,380 ft., NOTIFIED "TAMMY" W/TXRRC AT 07:20 HRS ON 6/20/16 OF INTENT TO RUN AND CEMENT THIS PRODUCTION CASING STRING. PROD PROD CSG/CEMENT RUN CEMENT No SHUT IN HEAD AND MONITOR PRESSURE ON STANDPIPE FOR 12 HOURS. MAINTAIN PRESSURE BETWEEN 3000 psi AND 3150 psi 15:00 03: ,702 15,702 RIGGED DOWN "NINE" CEMENTING EQUIPMENT. FLUSHED THROUGH BOP STACK, CHOKE MANIFOLD AND LINES, PUMPED OUT CELLAR. PULL MOUSEHOLE, RIG UP SLINGS ON CATWALK FOR SKID, RIG DOWN FLOW LINE, CHANGE OUT POLLUTION PAN, RIGGED UP BOP WINCHES, WHILE WAITING ON CEMENT 03:00 05: ,702 15,702 BROKE AND RAISED STACK WITH "MCE" NIPPLE DOWN CREW, SET 5.5in CASING SLIPS WITH 20K OVER STRING WEIGHT OF 135K (SET155K ON SLIPS) PROD PROD CSG/CEMENT BOP/OTHER No PROD PROD CSG/CEMENT NIPPLE UP B.O.P./WELLHEAD No

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