Terrace Petroleum Corporation Cunning Wolf UL No. 602H, 1980 FNL and 467 FWL Section 6, Block 23, ULS Pecos County, Texas
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1 Terrace Petroleum Corporation Cunning Wolf UL No. 602H, 1980 FNL and 467 FWL Section 6, Block 23, ULS Pecos County, Texas DAY 1 Previously built location, roads, built and lined reserve pits. Move in and rig up Precision 553. Approximately 40% moved DAY 2 Continue moving in Precision 553. All rig components moved in and derrick set on sub. The sub and derrick will be raised in the morning. Anticipated spud Sunday. The rig will break tour starting 3/30/13/ DAY 3 Continue MIRU Precision 553. Raise derrick and sub structure at 10 a.m. Continue rigging up and plugging in all components. MIRU Permian Premix Pit, bulk tanks and 4 frac tanks for mud storage and mixing. Anticipate spudding this afternoon DAY 4 RU centrifugal pumps on pits and fill with fresh water. RU pipecat catwalk. Tighten union and dresser sleeves between pits and function test catwalk. Install 20 conductor riser on 20 pre-set conductor, install turnbuckles and flowline. Install shaker screens, calibrate blocks, MD Totco and pump psi. Service top drive and change out swivel packing. Mix spud mud, pick up mouse hole shuck, RU 2 fill up line and function test pumps and top drive. RU geranimo line. Pre spud safety meeting and rig inspection. Strap and caliper BHA #1. Pick up 17.5 bit and BHA #1. Tag cement at 105 and drill out cement in conductor. Spud in at 1:00 p.m. 3/31/13. 4/1/13 drill from 120 to 172 at 8.6 fph. RPM WOB all DAY 5 At 6:00 A.M. on Depth = 810, Progress = 638, Present Operation = Service Rig. Drill from 172 to 810, survey at 436 Dev = 1.0 degrees, survey at 680 Dev = 1.0 degrees. Formation = Surface, MW = 9.1#/gal, Visc = 40, ph = DAY 6 At 6:00 A.M. on Depth = 1327, Progress = 517, Present Operation = Service Rig. Drill from 810 to 1327, survey at Dev = 0.7 degrees, survey at 1230 Dev = 0.4 degrees. Formation = Surface, MW = 9.1#/gal, Visc = 40, ph = DAY 7 At 6:00 A.M. on Depth = 1640, Progress = 313, Present Operation = Circulate and condition hole for surface casing procedures. Drill from 1327 to 1640, circulate and condition the hole for surface casing procedures. Formation = Surface, MW = 9.1#/gal, Visc = 40, ph = 8.0.
2 DAY 8 At 6:00 A.M. on Depth = 1640, Progress = 0, Present Operation = WOC. Formation = Surface, MW = 9.1 #/gal, Visc = 40, ph = 8.0. Casing details as follows: 1 (1.00 ) Texas Pattern Shoe 1 Joint (39.55 ) 13 3/8, 54.5#, J55 STC casing 1 Float Collar (0.80 ) 41 Joints ( ) 13 3/8, 54.5#, J-55 STC casing Total Pipe = ( ) set at DAY 9 At 6:00 A.M. on Depth = 1640, Progress = 0, Present Operation = Trip in hole. Cut off conductor and casing and weld on wellhead, NU BOP and choke line, TIH. Formation = Surface, MW = 8.4 #/gal, Visc = 29, ph = DAY 10 At 6:00 A.M. on Depth = 2680, Progress = 1040, Present Operation = Drilling Ahead. Drill cement, float collar and shoe, tag cement at 1596, tag float collar at 1597, drill cement from 1598 to 1640, Drill from 1640 to 2680 survey s at 1680 Dev = 2.5 degrees, 1951 Dev = 2.0 degrees, 2222 Dev = 1.1 degrees, 2402 Dev = 1.3 degrees and 2582 Dev = 1.3 degrees. Formation = Yates, MW = 8.4 #/gal, Visc = 29, ph = DAY 11 At 6:00 A.M. on Depth = 3273, Progress = 493, Present Operation = TOH to change bit and motor. Drill from 2685 to 3273 survey s at 2763 Dev = 1.3 degrees, 2943 Dev = 1.6 degrees and 3214 Dev = 1.2 degrees. Formation = Queen, MW = 9.1 #/gal, Visc = 29, ph = DAY 12 At 6:00 A.M. on Depth = 3713, Progress = 440, Present Operation = Drilling Ahead. Drill from 3273 to 3713 survey s at 3214 Dev = 1.2 degrees, 3485 Dev = 1.7 degrees and 3665 Dev = 1.5 degrees. Formation = Queen, MW = 9.4 #/gal, Visc = 29, ph = DAY 13 At 6:00 A.M. on Depth = 4526, Progress = 813, Present Operation = Drilling Ahead. Drill from 3713 to 4526 survey s at 3846 Dev = 1.3 degrees, 4026 Dev = 1.6 degrees, 4206 Dev = 1.9 degrees and 4386 Dev = 1.2 degrees. Formation = Delaware, MW = 9.1 #/gal, Visc = 45, ph = DAY 14 At 6:00 A.M. on Depth = 5385, Progress = 859, Present Operation = Drilling Ahead. Drill from 4526 to 5385 survey s at 4566 Dev = 1.2 degrees, 4746 Dev = 1.0 degrees, 4927 Dev = 1.3 degrees, and 5288 Dev = 0.4 degrees. Formation = Delaware, MW = 8.9+ #/gal, Visc = 42, ph = 9.
3 DAY 15 At 6:00 A.M. on Depth = 6064, Progress = 679, Present Operation = Circulate and TOH. Drill from 5385 to 6064 survey s at 5468 Dev = 0.7 degrees, 5649 Dev = 1.1 degrees, 5830 Dev = 1.1 degrees, and 6011 Dev = 2.6 degrees. Formation = Bone Springs Lime, MW = 8.9+ #/gal, Visc = 46, ph = DAY 16 At 6:00 A.M. on Depth = 6220, Progress = 156, Present Operation = Drilling Ahead. Slide drill from 6064 to 6089, rotate drill from 6089 to 6220, survey at 6101 Dev = 1.7 degrees. Formation = Bone Springs Lime, MW = 8.9+ #/gal, Visc = 43, ph = DAY 17 At 6:00 A.M. on Depth = 6427, Progress = 207, Present Operation = Trip in hole. Drill from 6220 to 6427, survey s at 6191 Dev = 1.5 degrees and 6371 Dev = 1.8 degrees. Formation = Bone Springs Lime, MW = 8.8+ #/gal, Visc = 41, ph = DAY 18 At 6:00 A.M. on Depth = 7360, Progress = 933, Present Operation = Drilling Ahead. Drill from 6427 to 7360, survey s at 6552 Dev = 1.8 degrees, 6732 Dev = 1.1 degrees, 6912 Dev = 0.9 degrees and 7272 Dev = 0.9 degrees. Formation = Bone Springs A 1 Marker, MW = 8.9 #/gal, Visc = 44, ph = DAY 19 At 6:00 A.M. on Depth = 7388, Progress = 28, Present Operation = Continue Running 9 5/8 casing to Drill from 7360 to 7388, survey at 7388 Dev = 1.0 degrees, RU casing crew, run /8 casing. Formation = Bone Springs A 1 Marker, MW = 8.9 #/gal, Visc = 44, ph = DAY 20 At 6:00 A.M. on Depth = 7388, Progress = 0, Present Operation = Makeup Directional motor and MWD. Finish running 9 5/8 casing to 7388, WOC, set slips, cut off casing. Formation = Bone Springs A 1 Marker, MW = 8.9 #/gal, Visc = 44, ph = 8.5. Casing details as follows: 1 (25.00 ) Welded Float Guide Shoe and Shoe Joint 1 Float Collar (0.90 ) 34 Joints ( ) 9 5/8, 43.5# HCK l-80 LTC casing 142 Joints ( ) 9 5/8, 40#, HCK L-80 LTC casing Total Pipe = ( ) set at DAY 21 At 6:00 A.M. on Depth = 7388, Progress = 0, Present Operation = Testing BOP s and casing. Formation = Bone Springs A 1 Marker, MW = 10 #/gal, Visc = 48.
4 DAY 22 At 6:00 A.M. on Depth = 7557, Progress = 169, Present Operation = Slide Drilling from Formation = Bone Springs B Marker, MW = 10 #/gal, Visc = DAY 23 At 6:00 A.M. on Depth = 7770, Progress = 213, Present Operation = Slide Drilling at 7770, survey s at 7582 Az degrees, 7628 Az degrees, 7673 Az degrees and 7718 Az degrees. Formation = Bone Springs B Marker, MW = #/gal, Visc = DAY 24 At 6:00 A.M. on Depth = 7968, Progress = 198, Present Operation = Slide Drilling at 7968, survey s at 7763 Az degrees, 7808 AZ degrees, 7853 Az degrees and 7898 Az degrees. Formation = Bone Springs C-1 Marker, MW = 9.9 #/gal, Visc = DAY 25 At 6:00 A.M. on Depth = 8082, Progress = 114, Present Operation = TIH with new bit, motor & BHA to 1450, slide drilling from 7968 to 8082, survey s at 7943 Az degrees, 7988 Az degrees and 8033 Az degrees. Formation = Bone Springs C-1 Marker, MW = 9.9 #/gal, Visc = DAY 26 At 6:00 A.M. on Depth = 8230, Progress = 148, Present Operation = Slide drilling at Survey s at 8078 Az degrees, 8123 Az degrees and 8169 Az degrees. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = DAY 27 At 6:00 A.M. on Depth = 8487, Progress = 257, Present Operation = Drilling (rotate) at Survey s at 8214 Az degrees, 8259 Az degrees, 8304 Az degrees, 8349 Az degrees and 8394 Az degrees. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = DAY 28 At 6:00 A.M. on Depth = 8660, Progress = 173, Present Operation Circulating bottoms TD, 8660 after short trip. Survey s at 8439 Az degrees, 8484 Az degrees, 8529 Az degrees, 8548 Az degrees and 8610 Az degrees. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = DAY 29 At 6:00 A.M. on Depth = 8660, Progress = 0, Present Operation = Running 7 liner. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = DAY 30 At 6:00 A.M. on Depth = 8660, Progress = 0, Present Operation = Changing BOP Rams. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = 50.
5 DAY 31 At 6:00 A.M. on Depth = 8660, Progress = 0, Present Operation = Drilling liner collar. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = DAY 32 At 6:00 A.M. on Depth = 9186, Progress = 526, Present Operation = Drilling lateral. Survey s at azm degrees, azm degrees, azm 90.1 degrees, azm degrees, azm degrees, azm degrees and azm degrees. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = DAY 33 At 6:00 A.M. on Depth = 10,031, Progress = 845, Present Operation = Drilling lateral. Survey s at azm degrees, azm degrees, azm degrees, azm degrees and azm 91.2 degrees. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = DAY 33 At 6:00 A.M. on Depth = 11,134, Progress = 1103, Present Operation = Rig Service. Survey s at 10, azm degrees, 10, azm degrees, 10, azm degrees, 10, azm degrees, 10, azm degrees and 10, azm 90.9 degrees. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = DAY 34 At 6:00 A.M. on Depth = 12,186, Progress = 1052, Present Operation = Rig Service. Survey s at 11, azm degrees, 11, azm degrees, 11, azm degrees, 11, azm degrees and 12, azm degrees. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = DAY 35 At 6:00 A.M. on Depth = 12,607, Progress = 421, Present Operation = Trip in Hole. Survey s at 12, azm degrees, 12, azm degrees and 12, azm degrees. Formation = Wolfcamp A Shale, MW = 10.0#/gal, Visc = 51.
6 DAY 36 At 6:00 A.M. on Depth = 12607, Progress = 0, Present Operation = Rig Down. Formation = Wolfcamp A Shale, MW = 10.0 #/gal, Visc = 51. Casing details as follows: 1 (25.00 ) Welded Float Guide Shoe and Shoe Joint 1 Float Collar (0.90 ) 34 Joints ( ) 9 5/8, 43.5#, HCK L-80 LTC 142 Joints (5,973.27) 9 5/8 40# HCK L-80 LTC Total Pipe = ( ) set at 7388 Released rig at 4:00 a.m. today. Well off report until June 3, 2013.
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