February 8, Ms. Jamie Jun, Esq. Fromhold Jaffe & Adams 789 East Lancaster Avenue, Suite 220 Villanova, PA 19085

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WWW.TRAFFICPD.COM February 8, 2016 Ms. Jamie Jun, Esq. Fromhold Jaffe & Adams 789 East Lancaster Avenue, Suite 220 Villanova, PA 19085 Re: Kohelet Yeshiva School Lower Merion Township, Montgomery County, PA TPD# KOLF.00001 Dear Jamie: At the last hearing, questions were raised as to whether the inclusion of certain additional data or alternative assumptions described below would have any material effect on the information shown in Tables 9 and 10 in our Traffic Study dated January 21, 2016. We have gone through this exercise and enclose Tables 9 and 10 modified to show the impacts of (1) conflicting pedestrians; (2) peak hour factor for the Old Lancaster Road and Exit-Only Site Driveway intersection using the manual counts at that intersection rather than using the peak hour factor at the Old Lancaster Road and N. intersection; and (3) use of uniform ideal flow rates of 1800 passenger vehicles per hour per lane in the peak hour rather than the rates of both 1800 and 1900. As you can see, the tables are not materially affected by any of these adjustments and levels of service at all studied intersections including the Old Lancaster Road and Exit-Only Site Driveway intersection are entirely unaffected. Indeed, inclusion of conflicting pedestrians seldom impacts levels of service certainly not at the low numbers here. Use of the peak hour factor for the Old Lancaster Road and Exit- Only Site Driveway intersection rather than the peak hour factor for the Old Lancaster Road and N. intersection results in a peak hour factor that tends to improve, rather than lower the level of service at the Old Lancaster Road and Exit-Only Site Driveway intersection. This demonstrates the reasonableness of our judgment to use the peak hour factor for the Old Lancaster Road and N. Highland Avenue intersection as the peak hour factor for the Old Lancaster and Exit-Only Driveway intersection. Also, as expected, use of 1800 as the uniform ideal flow rate, rather than 1900 in the one instance where 1900 was used, has no impact on the level of service since the studied road volumes do not come even close to 1800 vehicular trips. Also enclosed are worksheets that show the level of service that would result from use of projected future volumes as found in the Traffic Impact Study prepared by Horner and Canter Associates dated October 20, 2015 but using the Highway Capacity Manual 2010 Edition methodology. This shows that the level of service at the Old Lancaster Road and Exit-Only Driveway intersection post development remain at LOS C or better. Finally, I have confirmed that the heavy vehicles noted in the traffic counts that entered and exited the Kohelet driveways were school buses only. 2500 East High Street, Suite 650 Pottstown, PA 19464 610.326.3100 TrafficPD@TrafficPD.com

Ms. Jamie Jun, Esq. February 8, 2016 Page 2 Please let me know if you require any further information. Sincerely TRAFFIC PLANNING AND DESIGN, INC. Greg Richardson, P.E. Executive Vice-President grichardson@trafficpd.com Attachments cc: Holly Cohen Fred Fromhold, Esq. 2500 East High Street, Suite 650 Pottstown, PA 19464 610.326.3100 TrafficPD@TrafficPD.com DATE / Page 2

Old Lancaster Road & Exit-Only Site Driveway N. & Enter-Only Site Driveway TABLE 9 LEVEL OF SERVICE (SECONDS) SUMMARY Weekday AM Peak Hour Weekday PM Peak Hour 2017 Opening Year 2017 Opening Year EB L/T/R C C C B B B WB L/T/R C C C C C C NB L/T/R A A A A A A SB L/T/R A A A A A A ILOS A (8.7) A (8.7) A (9.1) A (9.3) A (9.3) A (9.4) EB L/R B B C B B C ILOS A (0.4) A (0.4) A (2.0) A (0.8) A (0.8) A (2.4) EB L A A A A A A ILOS A (0.5) A (0.5) A (0.6) A (0.2) A (0.2) A (0.4) Base = No-Build scenario; Projected = Build scenario; ILOS = Overall Level of Service Old Lancaster Road & Exit-Only Site Driveway N. & Enter-Only Site Driveway TABLE 9 (REVISED) LEVEL OF SERVICE (SECONDS) SUMMARY Weekday AM Peak Hour Weekday PM Peak Hour 2017 Opening Year 1 2017 Opening Year 1 EB L/T/R C C C B B B WB L/T/R C C C C C C NB L/T/R A A A A A A SB L/T/R A A A A A A ILOS A (8.7) A (8.7) A (9.1) A (9.3) A (9.3) A (9.4) EB L/R B B C B B C ILOS A (0.4) A (0.4) A (2.0) (2.1) A (0.8) (0.7) A (0.8) (0.7) A (2.4) (2.2) EB L A A A A A A ILOS A (0.5) A (0.5) A (0.6) A (0.2) A (0.2) A (0.4) Base = No-Build scenario; Projected = Build scenario; ILOS = Overall Level of Service 1. 2017 Opening Year = Student Population of 360 in 2017 2/4/16

Old Lancaster Road & Exit-Only Site Driveway N. & Enter- Only Site Driveway TABLE 10 95 TH PERCENTILE (FEET) SUMMARY 2017 Opening Year Available Weekday AM Peak Hour Weekday PM Peak Hour Storage EB L/T/R 250+ 93 93 50 50 WB L/T/R 250+ 83 95 128 138 NB L/T/R 250+ 120 145 123 135 SB L/T/R 250+ 143 200 133 173 EB L/R 200+ <25 25 <25 33 EB L 200+ <25 <25 <25 <25 Old Lancaster Road & Exit-Only Site Driveway N. & Enter- Only Site Driveway TABLE 10 (REVISED) 95 TH PERCENTILE (FEET) SUMMARY 2017 Opening Year 1 Available Weekday AM Peak Hour Weekday PM Peak Hour Storage EB L/T/R 250+ 93 93 50 50 WB L/T/R 250+ 83 95 128 138 NB L/T/R 250+ 120 145 123 135 SB L/T/R 250+ 143 200 133 173 EB L/R 200+ <25 25 30 <25 33 30 EB L 200+ <25 <25 <25 <25 1. 2017 Opening Year = Student Population of 360 in 2017 2/4/16

Analysis of Exiting Driveway Utilizing Horner & Canter Input Data and 2010 HCM Methodology 2017 Projected Conditions - Horner Canter Numbers and Inputs Timing Plan: AM Peak Hour 2017 Projected Conditions - Horner Canter Numbers and Inputs Timing Plan: AM Peak Hour Lane Group EBL EBR NBL NBT SBT SBR Lane Configurations Volume (vph) 46 68 0 304 520 0 Ideal Flow (vphpl) 1800 1800 1800 1800 1800 1800 Lane Width (ft) 16 12 12 14 12 12 Link Speed (mph) 15 35 35 Link Distance (ft) 260 385 1407 Travel Time (s) 11.8 7.5 27.4 Confl. Peds. (#/hr) 6 8 8 6 Peak Hour Factor 0.89 0.89 0.89 0.89 0.89 0.89 Heavy Vehicles (%) 10% 10% 0% 4% 4% 0% Parking (#/hr) 0 Shared Lane Traffic (%) Summary Area Type: Other Int Delay, s/veh 2.2 EBL EBR NBL NBT SBT SBR Vol, veh/h 46 68 0 304 520 0 Conflicting Peds, #/hr 6 8 8 0 0 6 Sign Control Stop Stop Free Free Free Free RT Channelized - None - None - None Storage Length 0 - - - - - Veh in Median Storage, # 0 - - 0 0 - Grade, % 0 - - 0 0 - Peak Hour Factor 89 89 89 89 89 89 Heavy Vehicles, % 10 10 0 4 4 0 Mvmt Flow 52 76 0 342 584 0 Major/Minor Minor2 Major1 Major2 Conflicting Flow All 934 600 592 0-0 Stage 1 592 - - - - - Stage 2 342 - - - - - Critical Hdwy 6.5 6.3 4.3 - - - Critical Hdwy Stg 1 5.5 - - - - - Critical Hdwy Stg 2 5.5 - - - - - Follow-up Hdwy 3.1 3.2 3 - - - Pot Cap-1 Maneuver 313 508 750 - - - Stage 1 600 - - - - - Stage 2 795 - - - - - Platoon blocked, % - - - Mov Cap-1 Maneuver 307 500 744 - - - Mov Cap-2 Maneuver 307 - - - - - Stage 1 595 - - - - - Stage 2 788 - - - - - Approach EB NB SB HCM Control Delay, s 18.2 0 0 HCM LOS C Minor Lane/Major Mvmt NBL NBT EBLn1 SBT SBR Capacity (veh/h) 744-399 - - HCM Lane V/C Ratio - - 0.321 - - HCM Control Delay (s) 0-18.2 - - HCM Lane LOS A - C - - HCM 95th %tile Q(veh) 0-1.4 - - Page 1 Page 2

Analysis of Exiting Driveway Utilizing Horner & Canter Input Data and 2010 HCM Methodology 2017 Projected Conditions - Horner Canter Numbers and Inputs Timing Plan: Weekday PM Peak 2017 Projected Conditions - Horner Canter Numbers and Inputs Timing Plan: Weekday PM Peak Lane Group EBL EBR NBL NBT SBT SBR Lane Configurations Volume (vph) 48 73 0 343 379 0 Ideal Flow (vphpl) 1800 1800 1800 1800 1800 1800 Lane Width (ft) 16 12 12 14 12 12 Link Speed (mph) 15 35 35 Link Distance (ft) 260 385 1407 Travel Time (s) 11.8 7.5 27.4 Confl. Peds. (#/hr) 17 8 8 17 Peak Hour Factor 0.89 0.89 0.89 0.89 0.89 0.89 Heavy Vehicles (%) 10% 10% 0% 1% 1% 0% Parking (#/hr) 0 Shared Lane Traffic (%) Summary Area Type: Other Int Delay, s/veh 2.3 EBL EBR NBL NBT SBT SBR Vol, veh/h 48 73 0 343 379 0 Conflicting Peds, #/hr 17 8 8 0 0 17 Sign Control Stop Stop Free Free Free Free RT Channelized - None - None - None Storage Length 0 - - - - - Veh in Median Storage, # 0 - - 0 0 - Grade, % 0 - - 0 0 - Peak Hour Factor 89 89 89 89 89 89 Heavy Vehicles, % 10 10 0 1 1 0 Mvmt Flow 54 82 0 385 426 0 Major/Minor Minor2 Major1 Major2 Conflicting Flow All 828 451 443 0-0 Stage 1 443 - - - - - Stage 2 385 - - - - - Critical Hdwy 6.5 6.3 4.3 - - - Critical Hdwy Stg 1 5.5 - - - - - Critical Hdwy Stg 2 5.5 - - - - - Follow-up Hdwy 3.1 3.2 3 - - - Pot Cap-1 Maneuver 364 620 845 - - - Stage 1 710 - - - - - Stage 2 758 - - - - - Platoon blocked, % - - - Mov Cap-1 Maneuver 350 604 838 - - - Mov Cap-2 Maneuver 350 - - - - - Stage 1 697 - - - - - Stage 2 744 - - - - - Approach EB NB SB HCM Control Delay, s 15.8 0 0 HCM LOS C Minor Lane/Major Mvmt NBL NBT EBLn1 SBT SBR Capacity (veh/h) 838-469 - - HCM Lane V/C Ratio - - 0.29 - - HCM Control Delay (s) 0-15.8 - - HCM Lane LOS A - C - - HCM 95th %tile Q(veh) 0-1.2 - - Page 1 Page 2