Gas Forces on Disc Valves

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Purdue University Purdue e-pubs nternational Compressor Engineering Conference School of Mechanical Engineering 1980 Gas Forces on Disc Valves J. Fleming J. Brown R. Davidson Follow this and additional works at: http://docs.lib.purdue.edu/icec Fleming, J.; Brown, J.; and Davidson, R., "Gas Forces on Disc Valves" (1980). nternational Compressor Engineering Conference. Paper 420. http://docs.lib.purdue.edu/icec/420 This document has been made available through Purdue e-pubs, a service of the Purdue University Libraries. Please contact epubs@purdue.edu for additional information. Complete proceedings may be acquired in print and on CD-ROM directly from the Ray W. Herrick Laboratories at https://engineering.purdue.edu/ Herrick/Events/orderlit.html

GAS FORCES ON DSC VALVES John Fleming, Lecturer James Brown, Reader Robert Davidson, Lecturer Department of Dynamics and Control University of Strathclyde, Glasgow, Scotland ABSTRACT This paper describes the measurement of the force exerted by the gas on a model disc valve as the gas escapes from the valve due to the disc being pulled from the stationary valve seat. The work forms part of a wider investigation of the aerodynamics of disc valves and reference is made to this. NTRODUCTON n previously reported work (1) it was found expedient to simulate the valve opening phase by withdrawing the plenum cylinder from a fixed valve disc. t was felt that this method did not exactly reproduce the flow past a moving valve and that, if possible, measurements should be made with a moving valve and fixed seat. This is particularly important when considering measurement of gas forces on the valve while the valve is fluttering. The moving valve apparatus is shown diagrammatically in Fig. 1. EXPERMENTAL EQUPMENT The main difficulty with the method of force meast.:i."ement described here is the occurrence of the unwan ted signal which results from the fact that the valve disc/transducer assembly is accelerating; i.e. the inertia force effects which, for much of the time, will be much greater in magnitude than the :force exerted by the gas. Different methods of measuring the gas :force were considered but all suffered from this disadvantage. Quartz piezoelectric transducers were chosen :for several reasons, including: a) a high natural frequency, b) high stability, c) linearity over the entire working range. The unwanted inertia force signal was dealt with by "cancelling it out", so to speak, with an equal and opposite inertia :force signal :from a nominally identical force transducer/disc valve assembly mounted back to back with the main force transducer. This "compensation" transducer is indicated in Fig. 1. Separate charge amplifiers were used :for each :force transducer, with a summing junction at the output (Fig. 2). ~-' allowed adjustment of the gain of the compensating amplifier so that maximum cancellation of acceleration effects could be achieved. Ei..ECTRO MECH/\N CAL ACTUATOR +COMPE\.!SATNC,. FORCE TRANSDUCER -FORCE TRAr-lSD UCEr~ FG. 1. DAGf~AM OF TEST RG 378

t was not possible to achieve total cancellation, since unavoidable minor asymmetries of the rig led to s~all differential transverse motions of the transducers. The gas force signal to noise ratio so achieved was satisfactory for most purposes. However, any residual unwanted signal can be removed by digital subtraction. This is possible due to the highly repeatable nature of the experimental results from one test to the next. The unwanted signal can, of course, be measured by operating the apparatus with zero gas flow. The recorded signal would be digitised and then subtracted from the previously digitised signal recorded during a test with air. The resulting signal should represent the effect of the air alone. Since the authors are still developing this technique, and its associated computer program, the results given in this paper were obtained by manual processing of the data. Valve displacement was measured by means of a capacitive transducer, which was calibrated by making use of slip gauges. Plenum pressure variations were measured by a piezoelectric pressure transducer. A calibrated pressure gauge was used to determine mean and datum levels. The electro-mechanical actuator could be employed either to hold the valve down on its seat, or to vibrate the valve. A de supply was provided both to provide the holding down force, and to set the mean position during oscillation. A superimposed ac supply gave oscillation at chosen frequencies. FoRC TllANs~uce.ll,- COMPE.NSA'TN'i' TRFNS])UCER. J ANP/...!FE_R. C/-!AR.GE AMf'LF! 1<.-S SUMMNG JUNCTON DODE CUT-OFr +~,.~~v H. F ;:: L T R (1'1CTiVE) The authors are also currently developing a hot wire anemometer system to enable the variation of gas velocity to be determined in magnitude and direction at stations in close proximity to the valve disc, as the disc moves relative to the seat either in flutter or in a transient pull-off test. The system is described elsewhere (2). TEST RESULTS The force measurements at fixed increments of valve lift (see Fig. 4) were made by setting the plenum pressure to the desired value (in this case 6 or 12 psi) and then recording the force signal which is obtained when the air is suddenly switched off. The force measuring system was calibrated using a Kistler charge calibrator (type 5351). The force transducers and the charge amplifiers were also made by Kistler. These steady-state values of force were compared with the gas force on the valve during a transient pull-off motion. Hard copies of typical oscilloscope traces of displacement and force for pull-off tests are shown in Fig. 3. The graphs of force against displacement derived from these traces are shown in Fig. 4. T1w features of the graphs shown in Fig. 4 seem worthy of comment. The first'is that the force during the transient pull-off test in the very early stage of opening, is significantly smaller than the corresponding force caused by steady-state flow with the valve lift fixed at that small opening. This FG 2 H. F, FL.,T R (PA.S<;!VE) r--...,,.--;d=-1 S P/..A C E M F._-N T StG,NAL "DUAL_- 13 A"1 1>-1 G T -4 L S TORA G 'DH=fl TSE.R OSC/t.._lOSCOPiS READ- OUT FORCE fviea::.vr//'-!g SYSTEM 379

Fl~. J, TYPCAL OSCLLOSCOPE. TR.ACE.S.... l'"l,.,.. ~;: : ~ ~ ~ ~ ~ 0 ~ ~ ~ ~ n ~ ~ ~ ~ 1 ~ ~ A ~ ~ ~ ~ ~ ~? ry ~ ~ ~.....,.,.~'-,,~~lm1ffif@jff_ft~'lie_--nn -.~,~.. r;;"'fmw :J~E!' -:~ ~. '. -hrs?,.ac~.. -'----- 1' ' ' J '.... : L-,. ~ -~-~----~...:.,... _ - - --- -- -&~-~----~-,_ i J - - 1 ---,. u, ;-. ' - ~ '., r-msl A- - '$' --...,.._!. ' _j - --. FG. 4. GAS ~ORCE: Y VALVE LF"i ' L 7STEADY FLOW AT FX::O O NCREMENTS or= VALVE. LF'T 1 5 STE:ADY FLOW AT NCREMENS OF VALVE LFT ~ TRANSENT PULL-oFF' TEST n-- -U r! O - 1 0./PQ S5. DFF. X PORT AREA _1 ----------- PRESS. DlFF. x Po>ZT AZE:A TRANSENT PU...i--OF~:: TFST 0 Q.t 0 '2 0 3 VAL-VE LFT (mm) 0 r- 0 0 -- ~- ----------- -...:.-~ ~.,.QiL8 n o ~--'------'------=..:...,---''"-,, L_~_._-~ 0 0-1 0 '2 VALVE LFT (ml"r\) 6 p.s.i. 1'2 p.s.-l. 380

was a feature reported by Brown et al (1) in 1976 and is confirmed here. The most likely explanation for this is that in steady flow the gas has established a significant pressure over the annular overlap region, whereas in the transient pull-off test starting from the closed position, in 0.5 ms or so, the gas has not had enough time to establish such a large pressure in this region. The second feature is that the gas force in both the steady-state and transient tests passes through a minimum value for a pressure difference of 6 psi but not for 12 psi. This apparently pressure dependent phenomenon remains unexplained. t is hoped that the hot wire anemometer program will shed some light on the problem. t appears that at a valve lift of around 0.23 mm, an abrupt change in flow pattern occurs for a pressure of 6 psi. When the pressure difference is 6 psi and the valve is closed, there is very close agreement between the measured value of gas force and that calculated by multiplying the port area by the pressure difference. n the case of 12 psi the measured force is higher than the value calculated in this way. This is almost certainly due to the sealing of the valve partially breaking down at 12 psi. This would expose part of the annular sealing area to gas pressure. The result would be a gas force on the valve in excess of the value given by pressure times port area. REFERENCES 1. Brown, J., Davidson, R. and Hallam W. Dynamic Measurement of Valve Lift Force, Purdue Compressor Technology Conference, Purdue University, 1976. 2. Brown, J., Davidson, R. and Fleming, J.S. Dynamic Performance of Automatic Compressor Valves, nternational Congress of Refrigeration, Venice, 1979. 381