Aircraft Fuel Cell Repair Equipment

Similar documents
M2.50-cal. Multishot Capabilities at the US Army Research Laboratory

DoD Coral Reef Protection and Management Program

AN EXPERIMENTAL INVESTIGATION OF SPILLING BREAKERS

z Interim Report for May 2004 to October 2005 Aircrew Performance and Protection Branch Wright-Patterson AFB, OH AFRL-HE-WP-TP

Stability & Control Aspects of UCAV Configurations

Remote Monitoring of Dolphins and Whales in the High Naval Activity Areas in Hawaiian Waters

Using SolidWorks & CFD to Create The Next Generation Airlocks

AFRL-RX-WP-TP

Characterizing The Surf Zone With Ambient Noise Measurements

Navy Shipbuilding Industrial Base

Internal Waves and Mixing in the Aegean Sea

Kelly Legault, Ph.D., P.E. USACE SAJ

Long-Term Autonomous Measurement of Ocean Dissipation with EPS-MAPPER

( max)o Wind Waves 10 Short Swell (large wave steepness) 25 Long Swell (small wave steepness) 75

High-Frequency Scattering from the Sea Surface and Multiple Scattering from Bubbles

BRRAKING WAVE FORCES ON WALLS

Temporary Flying Restrictions Due to Exogenous Factors

AFRL-RH-WP-TR

Air-Sea Interaction Spar Buoy Systems

Development of Low Volume Shape Memory Alloy Variable Ballast System for AUV Use

Examples of Carter Corrected DBDB-V Applied to Acoustic Propagation Modeling

DEVELOPMENT OF PRIMARY FRAGMENTATION SEPARATION DISTANCES FOR CASED CYLINDRICAL MUNITIONS

High Frequency Acoustical Propagation and Scattering in Coastal Waters

REPORT DOCUMENTATION PAGE

Waves, Bubbles, Noise, and Underwater Communications

Marine Mammal Acoustic Tracking from Adapting HARP Technologies

Waves, Turbulence and Boundary Layers

TITLE: Assessing the Hydrodynamic Performance of Fouling-Release Surfaces (ONR Research Contract # N WR )

Rogue Wave Statistics and Dynamics Using Large-Scale Direct Simulations

Frostbite in Ski Boots for Marines

Internal Waves in Straits Experiment Progress Report

Hydro-Thermal Vent Mapping with Multiple AUV's AZORES-2001

Imaging the Lung Under Pressure

REPORT DOCUMENTATION PAGE

OE Barricade Guide Development. Michelle Crull, PhD, PE Wallace Watanabe James Manthey, PE Charles Barker, PE

ADIABATIC INITIATION SENSITIVITY OF LIQUID ENERGETIC MATERIALS. Twenty-Seventh DOD Explosives Safety Seminar Las Vegas, Nevada August 1996

Global Ocean Internal Wave Database

Waves, Bubbles, Noise and Underwater Communications

Anthropogenic Noise and the Marine Environment

Welded Aluminum Fuel Tank Inspection for Pinhole Leaks. Fuel Tanks Delivered After 4/12/05 and before 2/06/06 on both Sportsman and GlaStar Aircraft

Inlet Influence on the Pressure and Temperature Distortion Entering the Compressor of an Air Vehicle

DOMESTIC PREPAREDNESS: PROTECTION FACTOR TESTING OF THE SE-SHIELD SUIT WITH THE SE400 POWERED AIR PURIFYING RESPIRATOR (PAPR)

Concrete Obstacle Vulnerability

Cost-Effectiveness of CC&D Measures and their Interaction

Behavioral Response of Dolphins to Signals Simulating Mid-Frequency Sonar

Acoustic Focusing in Shallow Water and Bubble Radiation Effects

TEST RESULTS OF AIR-PERMEABLE CHARCOAL IMPREGNATED SUITS TO CHALLENGE BY CHEMICAL AND BIOLOGICALWARFARE AGENTS AND SIMULANTS: EXECUTIVE SUMMARY

Observations of Near-Bottom Currents with Low-Cost SeaHorse Tilt Current Meters

Coastal Engineering Technical Note

Understanding the Dynamics of Shallow-Water Oceanographic Moorings

At-Sea Measurements of Diver Target Strengths at 100 khz: Measurement Technique and First Results

Three Dimensional Shallow Water Adaptive Hydraulics (ADH-SW3): Waterborne Vessels

Enhanced Passive Thermal Propulsion System

CITY AND COUNTY OF DENVER CR&CF RISK UNIT Compressed Gas Safety Standard

Diagnosing EVAP systems By: Bernie Thompson

Chemical Plume Mapping with an Autonomous Underwater Vehicle

THE EFFECTS OF ULTRAHIGH-PRESSURE WATERJET IMPACT ON HIGH EXPLOSIVES

Harbor Threat Detection, Classification, and Identification

TEST RESULTS OF PHASE 2 LEVEL A SUITS TO CHALLENGE BY CHEMICAL AND BIOLOGICAL WARFARE AGENTS AND SIMULANTS: EXECUTIVE SUMMARY

MIL-DTL-5886G Ballistic Fragmentation Qualification of the Carleton Life Support Systems Oxygen Cylinder, Part Number

TEST RESULTS OF PHASE 2 LEVEL B SUITS TO CHALLENGE BY CHEMICAL AND BIOLOGICAL WARFARE AGENTS AND SIMULANTS: EXECUTIVE SUMMARY

Exhibit 4. Determination of Static Pressure Performance of the Healy Clean Air Separator (Executive Orders VR-201-N and VR-202-N)

Aircrew Endurance and Effectiveness NACES Endurance Improvement

Observations of Velocity Fields Under Moderately Forced Wind Waves

STUDIES OF FINITE AMPLITUDE SHEAR WAVE INSTABILITIES. James T. Kirby. Center for Applied Coastal Research. University of Delaware.

Tagging and Playback Studies to Toothed Whales

Cover Page for Lab Report Group Portion. Pump Performance

Rip Currents Onshore Submarine Canyons: NCEX Analysis

AFRL-RI-RS-TR

NONLINEAR INTERNAL WAVES IN THE SOUTH CHINA SEA

INTERNATIONAL ASSOCIATION OF CLASSIFICATION SOCIETIES. Interpretations of the. IGF Code

Cruise Report Marine Mammal and Sea Turtle Observer UNDET Monitoring Hawaii Range Complex: 3 April 2014

Committee Input No. 35-NFPA [ Chapter 1 ] Submitter Information Verification. Committee Statement

Calculation of the Internal Blast Pressures for Tunnel Magazine Tests

REPORT DOCUMENTATION PAGE

AFRL-RH-WP-TP

CIRRUS AIRPLANE MAINTENANCE MANUAL

Determination Of Nearshore Wave Conditions And Bathymetry From X-Band Radar Systems

SPECIFICATIONS ATTENTION

Award Number: N

LOADED MULTICELLULAR MAGAZINE. Laurent ALLA IN

Distributed Integrated Ocean Prediction System (DIOPS) / SWAN Rapid Transition Program

Broadband acoustic transmission measurements in surface ship wakes

Fig. 2. M.I. Yaroslavtsev, 2002

Water Ingress Failure Analysis of Whistler II Unit

Right Whale Diving and Foraging Behavior in the Southwestern Gulf of Maine

Domestic Preparedness: Corn Oil Protection Factor (PF) Testing of Commercial Air-Purifying Negative Pressure Respirators with P-100 Filter Cartridges

The conversion of new certified central heating gas appliances must conform to directions outlined in this instruction.

Implementation of Structures in the CMS: Part IV, Tide Gate

Next Generation Modeling for Deep Water Wave Breaking and Langmuir Circulation

Natural Gas to L.P. Gas Conversion Kit

Installation Instructions

FTS SUBMERSIBLE PRESSURE TRANSMITTER USER S MANUAL

Canadian Light Source Inc. Vacuum Component Leak Test Technical Procedure

Shoreline Change Modeling Using One-Line Models: Application and Comparison of GenCade, Unibest, and Litpack

Your safety and the safety of others are very important.

METHOD 21 - DETERMINATION OF VOLATILE ORGANIC COMPOUND LEAKS. 1.2 Scope. This method is applicable for the

Tests of Level A Suits Protection Against Chemical and Biological Warfare Agents and Simulants: Executive Summary

RIP CURRENTS. Award # N

Determination of Nearshore Wave Conditions and Bathymetry from X-Band Radar Systems

Transcription:

Aircraft Fuel Cell Repair Equipment After Iniative Report AMB-05-005 PROJECT MANAGER: Capt John M. Yerger DSN 650-7608 john.yerger@mcguire.af.mil Air Force Air Mobility Battlelab DISTRIBUTION A. Approved for public release; distribution unlimited.

Report Documentation Page Form Approved OMB No. 0704-0188 Public reporting burden for the collection of information is estimated to average 1 hour per response, including the time for reviewing instructions, searching existing data sources, gathering and maintaining the data needed, and completing and reviewing the collection of information. Send comments regarding this burden estimate or any other aspect of this collection of information, including suggestions for reducing this burden, to Washington Headquarters Services, Directorate for Information Operations and Reports, 1215 Jefferson Davis Highway, Suite 1204, Arlington VA 22202-4302. Respondents should be aware that notwithstanding any other provision of law, no person shall be subject to a penalty for failing to comply with a collection of information if it does not display a currently valid OMB control number. 1. REPORT DATE 09 AUG 2006 2. REPORT TYPE After Initiative Report 3. DATES COVERED 00-09-2005 to 00-08-2006 4. TITLE AND SUBTITLE Aircraft Fuel Cell Repair Equipment (AFCRE) 5a. CONTRACT NUMBER 5b. GRANT NUMBER 5c. PROGRAM ELEMENT NUMBER 6. AUTHOR(S) John Yerger 5d. PROJECT NUMBER AMB-05-005 5e. TASK NUMBER 5f. WORK UNIT NUMBER 7. PERFORMING ORGANIZATION NAME(S) AND ADDRESS(ES) USAF Air Mobility Battlelab,5656 Texas Avenue,Fort Dix,NJ,08640 9. SPONSORING/MONITORING AGENCY NAME(S) AND ADDRESS(ES) USAF Air Mobility Battlelab, 5656 Texas Avenue, Fort Dix, NJ, 08640 8. PERFORMING ORGANIZATION REPORT NUMBER AMB-05-005 10. SPONSOR/MONITOR S ACRONYM(S) AMB 11. SPONSOR/MONITOR S REPORT NUMBER(S) AMB 12. DISTRIBUTION/AVAILABILITY STATEMENT Approved for public release; distribution unlimited 13. SUPPLEMENTARY NOTES 14. ABSTRACT PROBLEM: Aircraft fuel cell repair time is quite lengthy due to dated troubleshooting tools, sealant cure time and repair validation. PROPOSED SOLUTION: Use helium gas to troubleshoot leaks and validate repairs. Use new technology to remove and cure sealant. 15. SUBJECT TERMS Aircraft, fuel, cell, repair, equipment, helium, sealant, cure 16. SECURITY CLASSIFICATION OF: 17. LIMITATION OF ABSTRACT a. REPORT unclassified b. ABSTRACT unclassified c. THIS PAGE unclassified 18. NUMBER OF PAGES 10 19a. NAME OF RESPONSIBLE PERSON Standard Form 298 (Rev. 8-98) Prescribed by ANSI Std Z39-18

1. MISSION STATEMENT. 1.1. Problem/Situation. Aircraft fuel cell repair time is quite lengthy due to dated troubleshooting tools, sealant cure time and repair validation. 1.2. Proposed Solution. Use helium gas to troubleshoot leaks and validate repairs. Use new technology to remove and cure sealant. 1.3. Mission Impact. The system demonstrated has the potential to reduce troubleshooting man hours, repair man hours and sealant cure time. The equipment will potentially reduce non-mission capable time by 75%. 2. COURSE OF ACTION. 2.1. Strategy to Achieve. The concept demonstration occurred on a 305 AMW KC-10A and in the fuel cell repair hangar. Aerowing, Inc. provided the equipment used to troubleshoot and repair the fuel leak. The equipment consisted of the helitester, rapid desealer and rapid curing device. Aero Wing personnel trained two groups of Air Force fuel cell technicians on the equipment. The groups employed the equipment independent of each other. Following each demonstration, the technicians completed surveys. 2.1.1. Details. Aerowing, Inc., 2006 Gladstone Ave., Nashville, TN, provided equipment and personnel via a bailment agreement. The demonstration occurred on aircraft 87-0121. The discrepancy repaired was Fuel leak at #3 tank outboard fuel dipstick panel, class B. 2.2. Objective 1. Determine the helitester s ability to identify a leak path in a timely manner. 2.2.1. Method. Troubleshoot a known leak using current blow-back leak detection methods. Then troubleshoot the same leak using the helitester. 2.2.2. Results. The helitester configured for aviation application was not demonstrated. It failed the start up bit check and would not zero out. A helitester not configured for aviation application did demonstrate the potential for helium to be used as a troubleshooting method. A leak was simulated by passing helium through a fuselage drain hole. Then the helitester was used to identify the source of helium. Based on the technicians feedback, it is evident a better method for troubleshooting than currently used should be explored. The current method of using forced air and soapy water can be very time consuming and laborious. The technician s feedback on a helium troubleshooting tool was positive. Some comments were, with this item it cuts down time and could eliminate negative pressure test ; will save hours of blow back procedures ; and would save countless hours by eliminating the time it takes to cap off vent systems and open additional fuel tanks to perform positive and negative pressure checks. Survey results are shown in table 2.1. 1

Table 2.1 Helitester feedback survey results 5 4 3 2 1 0 2.3. Objective 2. Determine the rapid desealer s (RDS) ability to effectively remove sealant. 2.3.1. Method. Use the desealer tool to remove sealant from joints and fastener caps. 2.3.2. Results. The RDS was very efficient. Sealant was removed from a seam in 30 seconds. Normally it would have taken an hour using current methods to remove this sealant. The RDS is a pneumatic, reciprocating hand tool approximately 16 inches in length. A replaceable plastic tip threads onto the arm. This tip has a point with two different angles. These can be sharpened for reuse, until worn past a certain threshold. The access panel for the wing tip tank was removed from the aircraft and desealed on the workbench. A training board was also used. Sealant was removed from a.25 inch wide horizontal seam, a corner with rivets, a vertical seam on a horizontal joint and a 6 inch test strip. After all areas were desealed, only minor areas around fastners and corners required conventional cleanup. The technicians feedback was positive. Some comments were, desealer is large and access in areas could be difficult, for large areas the desealer is an excellent tool ; this is great for larger tanks like the #2 and #3 mains of the C-17A or the #2 main and upper center wing tanks of the KC-10A, but not the smaller tanks ; and ETIC s could be cut, price of the bits and durability could be a problem. Survey results are shown in table 2.2. 2

Rapid Desealer on work bench Table 2.2 RDS acceptability to remove sealant 4 3 2 1 0 2.4. Objective 3. Determine the rapid curing device s (RCD) ability to cure sealant at faster rate than stagnant conditions. 2.4.1. Method. Apply sealant to a mock-structure and use the rapid curing device to speed sealant cure time. 3

2.4.2. Results. PR1422B2NA, a B 1/2 sealant, was used for this demonstration. This sealant was cured in 30 minutes. Under normal conditions, the sealant requires 8 hours. Additionally, the sealant was tack free in 20 minutes; much faster than the normal 6 hours. With set-up and start-up time included, the sealant was cured within one hour. The RCD required approximately 15 minutes set-up time. This time was used to connect 3 inputs, 2 outputs, and 2 probes. Inputs are 110 volt power, air (50 cfps) and propane. Outputs are 28vDC and an air/propane mixture. The 2 probe leads provide temperature input from the sealant and the structure. Once equipment was in position a 10 minute start-up cycle initiated. The RCD was demonstrated on the training board because the control box is not intrinsically safe and not rated to be within 50 feet of the aircraft. Additionally, the hoses connecting the control box to the emitter heads are not long enough to keep the box outside the safe area. The emitter head/thermoreactor is intrinsically safe and certified for fuel cell environments. The technician s feedback was positive. Some comments were at that rate of cure time B2 sealant can be used which would give you a better repair ; curing of the sealant was rapid and the down time of an aircraft could be decreased ; and curing time is great preps didn t take long. Survey results are shown in table 2.3. RCD control box with propane, power, and air inputs 4

Table 2.3 RCD acceptability of time to cure sealant 5 4 3 2 1 0 2.5. Objective 4. Determine the rapid curing device s ability to cure sealant consistently through the sealant s mass. 2.5.1. Method. Examine sealant cured using the rapid curing device and evaluate for consistency of skin formation or air bubble formation. 2.5.2. Results. There was no skin formation or trapped air bubbles. The sealant was cured throughout the entire body. The temperature applied to the sealant ranged from 120 to 130 Fahrenheit. The RCD thermoreactor emission spectrum is nearly identical to the absorption spectrum of paints and sealants. It is this frequency concentration, not the heat, that accelerates the sealant curing. 5

Sealant being evaluated after curing 2.6. Objective 5. Determine the rapid curing device s functionality within the fuel tanks. 2.6.1. Method. Measure the distance from the rapid curing device to the sealant for distance and angle. 2.6.2. Results. Positioning the emitter head within most heavy aircraft will be possible. The emitter head was positioned with zero angle of deflection and ten inches from the sealant. The emitter head was suspended from a structure above the training board. The manufacturer procedures require line of sight and 8 to 12 inches for maximum effectiveness. Maximum distance recommended is 36 inches. The tip tank repair demonstration showed limited application for the RCD. The small internal dimensions and multiple piping in the tank offered few potential uses. However, the technicians unanimously agreed the RCD would be functional for the majority of heavy aircraft integral tank repairs. Aerowing provides multiple brackets designed for positioning. The technicians feedback was positive. Some comments were device is user friendly, easy to start and function, could be somewhat bulky and could be a problem depending on access to an area ; the hoses are my only concern ; and overall this is a great device and could be a great asset. Survey results are shown in table 2.4. 6

RCD positioning over training board Table 2.4 RCD acceptability of functionality within the fuel tanks 5 4 3 2 1 0 7

2.7. Objective 6. Determine the mapping kit s ability to pressurize the fuel system. 2.7.1. Method. Compare the pressure in the system to the mapping kit s instrumentation and the connections for leaking. 2.7.2. Results. The equipment was not demonstrated. The 327 CLSG did not approve its use and did not deem it applicable to the KC-10. 2.8. Objective 7. Determine the mapping kits ability to assist in troubleshooting. 2.8.1. Method. Verify helium moving through the leak path with the helitester. 2.8.2. Results. The equipment was not demonstrated. The 327 CLSG did not approve its use and did not deem it applicable to the KC-10.. 3. RESOURCES. 3.1. Schedule. Table 3.1. Initiative Schedule EVENT START FINISH Planning Jul 05 Dec 05 Demonstration Jan 06 Jan 06 After Initiative Report Jan 06 Mar 06 MAFROCC Coordination Feb 06 Mar 06 AMC/CV Transition Brief Mar 06 Mar 06 3.2. Funding. Table 3.2. Resources RESOURCE QUANTITY SOURCE TIMEFRAME EST COST Helitester 1 Aero Wing Jan 06 $0 Rapid Desealer 1 Aero Wing Jan 06 $0 Rapid Curing Device 1 Aero Wing Jan 06 $0 Travel 2 AMB Aug 05 Mar 06 $385.75 Total $385.75 3.3. Organizational Support. The AMC fuel cell functional manager provided subject matter expertise. The fuel cell lead engineer, 327 CLSG/GFLT, provided approval for using equipment not listed in technical orders. The 305 MXS provided aircraft and personnel to participate in the demonstration. 8

9