SUBSEA KILL SHEET EXERCISE No. 5

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Subsea Kill Sheet Exercise No. 5 SUBSEA KILL SHEET EXERCISE No. 5 Name: Date: Complete the Subsea vertical kill sheet provided on pages 2 and 3. Then answer questions 1 to 12. Please round calculations as per good well control practice. Well data : Hole size Hole depth (Below RKB) Casing shoe depth RKB to mean sea level (MSL) Internal capacities: Drill pipe Heavy wall drill pipe Drill collars Choke line Marine riser Annulus capacities: Drill collars in open hole Drill pipe and HWDP in open hole Drill pipe and HWDP in casing Drill pipe in Marine riser Mud pump data: Pump output at 98% volumetric efficiency Slow circulation rate data: @ 45 spm through the riser @ 45 spm through the choke line Other relevant information: Active surface fluid volume Drill pipe, 5 inch closed end displacement Seawater density Surface line volume Formation strength test data: Surface leak-off pressure with 10.0 ppg mud Kick Data: The well kicked at 6040 vertical depth Shut in drill pipe pressure Shut in Casing pressure Recorded pit gain Mud weight in hole 8 ½ inches 6,080 feet MD, 6040 ft TVD 9 5 / 8 inches, 5000 ft MD/TVD 50 feet 5 inch (S-135-NC50), capacity 0.0178 bbl/ft 5 inch, length 400 ft, capacity 0.0088 bbl/ft 6 ½ inch x 2 13 / 16 inch, length 600 ft, capacity 0.0077bbls/ft 3 inch ID, length 515 ft, capacity 0.0087 bbls/ft length 500 feet, capacity 0.3892 bbls/ft 0.0292 bbl/ft 0.0459 bbl/ft 0.0505 bbl/ft 0.3638 bbl/ft 0.102 bbl/stroke 400 psi 500 psi 460 bbl 0.0254 bbl/ft 8.6 ppg 14 bbls 1500 psi 600 psi 870 psi 19 bbls 10.4 ppg The well will be killed using the Wait and Weight method Answer the following TWELVE questions from the data above. The attached kill sheet may be used to assist you with your calculations Revised April 2012 1

Subsea Kill Sheet Exercise No.5 Revised April 2012 2

Subsea Kill Sheet Exercise No. 5 Revised April 2012 3

Subsea Kill Sheet Exercise No.5 1. Calculate the pressure safety margin at the casing shoe in this static condition, assuming the top of the kick is below the casing shoe. Answer psi 2. How many strokes are required to pump from pump to bit? Answer strokes 3. How many strokes are required to pump from the bit to casing shoe? Answer strokes 4. How much time is required to circulate the total well system volume? Answer minutes 5. How many strokes are required to displace the marine riser to kill fluid before opening the BOP? Answer strokes 6. What is the kill mud density? Answer ppg 7. What is the Initial Circulating Pressure? Answer psi 8. What is the Final Circulating Pressure? Answer psi Revised April 2012 4

Subsea Kill Sheet Exercise No. 5 9. What is the Initial dynamic casing pressure at kill pump rate? Answer psi 10. What is the MAASP after circulation of the kill mud? Answer psi 11. Calculate the pressure drop per 100 strokes of kill mud fluid pumped inside the drill string. Answer psi/100 strokes 12. If all the influx is at the bottom of the hole, calculate the gradient of the influx. Answer psi/ft Revised April 2012 5

Subsea Kill Sheet Exercise No.5 SUBSEA KILL SHEET EXERCISE NO. 5 Answers Before attempting to fill in the kill sheet, draw a simple sketch of the well to determine the total annulus lengths. An example is shown below. Only use measured depths and remember that total annulus length (including the choke line) may not equal measured depth if the Choke line length is greater than the Riser length. Revised April 2012 6

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SUBSEA KILL SHEET EXERCISE NO. 5 Answers 1. 508 psi Pressure Safety Margin = MAASP SICP = 1378 psi 870 psi = 508 psi 2. 1104 strokes From Kill Sheet, surface to bit strokes = 967 stokes Surface line strokes = 14 bbls 0.102 bbl/stroke = 137 strokes Pump to Bit stokes = 967 + 137 = 1104 strokes 3. 388 strokes 4. 80-81 minutes (80.6 minutes) 5. 1782-1786 strokes (1784 strokes) 6. 12.4 ppg 7. 1000 psi 8. 477 psi 9. 770 psi 10. 858 psi New MAASP = (Max. Allowable Mud Density Kill Mud Density) x 0.052 x TVD shoe = (15.7 ppg 12.4 ppg) x 0.052 x 5000 ft. = 858 psi 11. 54 psi/100 strokes = 239.2 feet Revised April 2012 12

12. Volume of Influx around Drill Collars = DC/OH annular capacity(bbls/ft) x DC Collar length = 0.0292 bbls/ft x 600 feet = 17.52 bbls Voulme of Influx around HWDP = Kick Volume - 17.52 bbls = 19 bbls 17.52 bbls = 1.48 bbls Height of Influx above Drill Collars = 1.48 bbls HWDP/OH annular capacity (bbls/ft) = 19 bbls 0.0459 bbls/ft = 32.2 feet Total Influx height = 600 + 32.2 feet = 632.2 feet Formation Pressure = SIDDP + HP string = 600 + (10.4 ppg x 0.052 x 6040 ft) = 600 psi + 3266.4 psi = 3866.4 psi HSP mud in annulus = 10.4 ppg x 0.052 x (6040 ft -632.2 ft) = 10.4 ppg x 0.052 x 5407.8 ft. = 2924.5 psi Kick Hydrostatic = Formation Pressure SICP HSP mud in annulus = 3866.4 psi 870 psi 2924.5 psi = 71.9 psi Gradient of Influx (psi/ft) = Kick Hydrostatic (psi) Height of Influx (ft) = 71.9 psi 632.2 feet = 0.113 psi/ft Revised April 2012 13

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