ENDEAVOR ENERGY RESOURCES Lease WELL NO FIELD PBTD PERFORATIONS FOREMAN TOOLPUSHER API NUMBER DATE University 5-20-21 #1H 14,223' Tony Cody 07/02/13 OART WEATHER FLUID SUMMARY W/O UNIT DATA W/L UNIT DATA CASING DATA VOLUMES WEIGHT (PPG) PV PIPE SIZE Csg wt/ grade CASING ID TBG VOLUME (BBLS) TOP OF FISH DAYS ON LOCATION PREVIOUS (CPS) $000 1 DAILY TYPE FLUID YP (#/100FT2) MAX PULL (70%) MAX PULL (100%) CASING BURST (100%)ANN VOLUME (BBLS) PREVIOUS TOF PROJECT DAYS LEFT CUMM $000 VIS (SEC) OIL (%) RKB-TH CORR RKB-TH CORR YEAR DRILLED TOT HOLE VOL (BBLS FISH LENGTH TARGET DAY COMP PROJECTED AMOUNT BHA (FT) BHA DESCRIPTION : LONG STRING (AM) SHORT STRING (AM) CASING (AM) DEPTH OVERPULL LENGTH FISH DESCRIPTION : LONG STRING (PM) SHORT STRING (PM) CASING (PM) PROJECT OBJECTIVE: Drill plugs and clean out to PBTDw/ Coil Tubing Unit BEG LOAD TODAY REC TOTAL REC LOAD REMAIN TIME DEPTH Fluid Rate ANNULUS 9:00 12:10 14:30 15:30 17:00 17:15 18:40 0 05 100 20:47 6000 25 500 22:35 14240 25 500 22:40 14230 25 500 1:00 0 0 0 DETAIL REPORT OF OPERATIONS AOL Wait On Well Head Valve Valve On Location RUCU Put On BHA Surface Test BHA SIH Weight Check - Raise Fluid Rate Tag Float Callor - Pick Up 10Ft POOH At Surface - Shut In/ Done For Day BEGINNING REPORT DATA TIME & DATE : ENDING REPORT DATA TIME & DATE :
ENDEAVOR ENERGY RESOURCES Lease WELL NO FIELD PBTD PERFORATIONS FOREMAN TOOLPUSHER API NUMBER DATE University 5-20-21 #1H 14,223' Tony Cody 07/03/13 OART WEATHER FLUID SUMMARY W/O UNIT DATA W/L UNIT DATA CASING DATA VOLUMES WEIGHT (PPG) PV PIPE SIZE Csg wt/ grade CASING ID TBG VOLUME (BBLS) TOP OF FISH DAYS ON LOCATION PREVIOUS (CPS) $000 2 DAILY TYPE FLUID YP (#/100FT2) MAX PULL (70%) MAX PULL (100%) CASING BURST (100%)ANN VOLUME (BBLS) PREVIOUS TOF PROJECT DAYS LEFT CUMM $000 VIS (SEC) OIL (%) RKB-TH CORR RKB-TH CORR YEAR DRILLED TOT HOLE VOL (BBLS FISH LENGTH TARGET DAY COMP PROJECTED AMOUNT BHA (FT) BHA DESCRIPTION : LONG STRING (AM) SHORT STRING (AM) CASING (AM) DEPTH OVERPULL LENGTH FISH DESCRIPTION : LONG STRING (PM) SHORT STRING (PM) CASING (PM) PROJECT OBJECTIVE: Drill plugs and clean out to PBTDw/ Coil Tubing Unit BEG LOAD TODAY REC TOTAL REC LOAD REMAIN TIME DEPTH Fluid Rate ANNULUS 8:30 9:50 10:36 0 05 0 11:23 6000 05 0 12:40 14215 1 0 12:50 14150 0 0 12:57 14086 0 0 13:05 14215 25 0 13:27 14215 25 0 13:40 14086 0 0 15:30 0 0 0 DETAIL REPORT OF OPERATIONS TCP Guns On Location/Rig Up Tool Assembly Regin Coil Unit - Stand By SIH Weight Check - Raise Fluid Rate Shut In Back Side/Raise Rate to 1bpm/Guns fire Guns Fire Guns Fire Start Pumping Acid Spot Acid on Formation Shut Pump Down/POOH At Surface - Shut In - Rig Down BEGINNING REPORT DATA TIME & DATE : ENDING REPORT DATA TIME & DATE :
University 5-20-21 #1H Joe Harrison 08/29/13 Thursday TOP OF FISH DAYS ON LOCATIONPREVIOUS $000 5 1/2" 17# DAILY $7,01500 TYPE FLUID YP (#/100FT2MAX PULL (70%AX PULL (100ASING BURST (100ANN VOLUME (BBL PREVIOUS TOF PROJECT DAYS LEFTCUMM $7,01500 VIS (SEC) OIL (%) RKB-TH CORRKB-TH CORRYEAR DRILLEDOT HOLE VOL (BBL TARGET DAY COMP PROJECTED AMOUNT LONG STRING (PM)SHORT STRING (PM) CASING (PM) PROJECT OBJECTIVE: TODAY REC TOTAL REC LOAD REMAIN TIME - TIME 40 Road Globe Rig 1 to Location FTP=0 Spot Reverse Unit Put Tubing & Racks on side of Location Park Logging Trucks on side of Location
University 5-20-21 #1H Joe Harrison 08/30/13 Thursday TOP OF FISH DAYS ON LOCATIONPREVIOUS $7,01500 5 1/2" 17# DAILY $17,90300 TYPE FLUID YP (#/100FT2MAX PULL (70%AX PULL (100ASING BURST (100ANN VOLUME (BBL PREVIOUS TOF PROJECT DAYS LEFTCUMM $24,91800 VIS (SEC) OIL (%) RKB-TH CORRKB-TH CORRYEAR DRILLEDOT HOLE VOL (BBL TARGET DAY COMP PROJECTED AMOUNT LONG STRING (PM)SHORT STRING (PM) CASING (PM) PROJECT OBJECTIVE: TODAY REC TOTAL REC LOAD REMAIN 9:00-11:00 20 ND Well Head on Both Wells Down to Master Valve 11:00-2:00 30 RU Jones Wire Line, PU Gauge Ring, Weight Bars & Collar Locator RIH to 6,000', Did not see Anything, POOH 2:00-4:30 25 PU 5 1/2" Wire Line Set AS1-X Watson Packer, With Rupture Disc, Set @ 6,350' POOH, PU 5 1/2" Wire Line Set RBP, RIH Set @ 5,700' Bleed Well Down, RU Basic Pumped 55 BBLS Fresh Water Pressured up to 1500 PSI Held "OK" for 15 Minutes, RD Basic 4L30-5:00 05 RD Jones SWI SD 5:00-6:00 10 Road Globe Rig 1 Crew to Midland
University 5-20-21 #1H 14,195' Joe Harrison 4232535136 09/03/13 Thursday TOP OF FISH DAYS ON LOCATIONPREVIOUS $24,91800 5 1/2" 17# P-110 DAILY $52,58500 TYPE FLUID YP (#/100FT2MAX PULL (70%AX PULL (100ASING BURST (100ANN VOLUME (BBL PREVIOUS TOF PROJECT DAYS LEFTCUMM $77,50300 VIS (SEC) OIL (%) RKB-TH CORRKB-TH CORRYEAR DRILLEDOT HOLE VOL (BBL TARGET DAY COMP PROJECTED AMOUNT icked Up By AccideLONG STRING (PM)SHORT STRING (PM) CASING (PM) PROJECT OBJECTIVE: TODAY REC TOTAL REC LOAD REMAIN RIH with Gas Lift Valves 6:00-8:00 20 Road Globe Rig 1 Crew to Location 8:00-11:00 30 Set Rig Mat, Set Pipe Racks, Put 198 Joints 2 7/8" J-55 Tubing RU WSU, Loaded Casing, Pressured Tested 5 1/2" 17# P-110 Casing to 5,100 PSI, For 15 Minutes Held "OK" 11:00-2:00 30 Ready to ND Frac Valve, NU BOP Spool from 10K to 5K We Had on Location Friday Got Picked up by Accident Had to wait on J & W to Bring another one 2:00-3:00 10 ND Frac Valve NU Spool & BOP 3:00-4:30 15 PU Over Shot RIH 4:30-6:00 15 While Running in the Hole Well did not Run Over Pumped about 15 BBLS well Circulated Gas & Oil Pumped 85 More BBLS Still Was not Solid Water Had Lots of Gas and some Oil SWI Will see if can Bleed it off in the Morning, And Reload it with Water or determine if we have a Problem 6>00-7:00 10 Road Globe Rig 1 Crew to Midland 130
University 5-20-21 #1H 14,195' Joe Harrison 4232535136 09/04/13 Wednesday TOP OF FISH DAYS ON LOCATIONPREVIOUS $77,50300 5 1/2" 17# P-110 DAILY $52,58500 TYPE FLUID YP (#/100FT2MAX PULL (70%AX PULL (100ASING BURST (100ANN VOLUME (BBL PREVIOUS TOF PROJECT DAYS LEFTCUMM $130,08800 VIS (SEC) OIL (%) RKB-TH CORRKB-TH CORRYEAR DRILLEDOT HOLE VOL (BBL TARGET DAY COMP PROJECTED AMOUNT icked Up By AccideLONG STRING (PM)SHORT STRING (PM) CASING (PM) PROJECT OBJECTIVE: TODAY REC TOTAL REC LOAD REMAIN RIH with Gas Lift Valves 6:00-8:00 20 Road Globe Rig 1 Crew to Location Well Was Full of Fluid, Pressured up to 2,000 PSI Held "OK" 15 Minutes 8:00-9:00 10 Latch onto RBP Set @ 5,700' 9:00-10:00 10 TOH (173 Joints) 2 7/8" J-55 Tubing PU BHA 1-5/2' AS1X Watson Packer, 1-187 " F" Nipple, 1-4' Sub, & 1-2 7/8" SN 10:00-11:30 15 TIH with 10 Gas Lift Valves, Latch into AS1-X Packer Set @ 6,350', 192 Joints ( (187 "F" Nipple in 15 Pts Compression) 11:30-12:00 05 ND BOP NU WH, Pumped out Rupture Disc 12:00-1:30 15 Pump 200 BBLS Fresh Water Down Tubing 2 BPM @ 500 PSI 1:30-2:30 10 RD WSU Move Out 85