Low Coking Temperatures & Recent Site Experience

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Delayed Coker Low Coking Temperatures & Recent Site Experience Presented by Mitch Moloney of ExxonMobil mitchell.j.moloney@exxonmobil.com @ Coking.com April-2010 MJ a Moloney - ExxonMobil April-2010 coking.com 0

Handling Coke Drums that have experienced Less-than-Required Coking Temperatures Logic Flow Diagram Recommended + Short-Run Drum => Oil Dilution & Drain to Blowdown System => Extended Steam Stripping & Quenching => Superheated Steam Stripping + Low Coking Temperatures => When to RETURN to coke drum => When to GET OUT of the coke drum MJ Moloney - ExxonMobil April-2010 coking.com 1

Short-Run Drum - Attendant Risks Risks of Not Properly Handling a Short-Run Drum: (1) If not properly stripped and cooled, there is risk of fire and explosion => Anacortes Coke Drum (2) Creating a complete mess on removing the bottom head, that can require a feed cut or train recirculation, if clean-up takes an extended period of time. => Also creates attendant safety risks MJ Moloney - ExxonMobil April-2010 coking.com 2

Creating a Mess (jul-2000): MJ Moloney - ExxonMobil April-2010 coking.com 3

Creating a Mess (jul-2000): MJ Moloney - ExxonMobil April-2010 coking.com 4

Creating a Mess (jul-2000): MJ Moloney - ExxonMobil April-2010 coking.com 5

s Anacortes Facilities => Provide an emergency fluid (e.g., water, gas oil, gas, etc.) to ensure coke drum inlet line and coke bed flow channels remain open, IF both steam and regular quench water sources are lost for an extended period of time during a power failure or other similar event. There are two alternatives: (1) Unplug the feed line when utilities back in service (2) Wait several weeks for the coke drum to cool This is a low probability event, which makes it difficult to justify an extensive facilities investment Several sites have justified connecting diesel-powered water or firewater via a low cost jumpover to their quench water line (requires special controls!) => Other sites are living with the alternatives MJ Moloney - ExxonMobil April-2010 coking.com 6

Short-Run Drum - Establish Site Criteria Based on Site Experience - Determine Time Criteria i thatt Ensures Completely Coked Resid Site 1 6-8 Site 2 4 Site 3 6-8 Site 4 6 Site 5 6-8 Site 6 4 Site 7 4 Site 8 12 MJ Moloney - ExxonMobil April-2010 coking.com 7

Short-Run Drum - Light Oil Dilution Repeated Oil Dilution to warm-up condensate drum, followed by steam stripping and normal water quench (1) Inject steam in bottom (2) Inject LGO through condensate drum and overhead quench, for same period of time as oil was in the drum (3) Agitate LGO with steam from bottom (can hear liquid) (4) Block in and drain to condensate drum (pull strainers from blowdown condensate pumps) (5) Continue washing and agitation until material is thinned out, based on visual inspection at the warm-up drum (6) Open little steam until blowdown is available (7) Open big steam for 30 minutes to blowdown (8) Cool drum with normal procedure MJ Moloney - ExxonMobil April-2010 coking.com 8

Short-Run Drum - Superheated Steaming Take Feed Out of train & pass steam through h coker heater to superheat it to +900 F in order to help finish the coking reactions => Disadvantage of this procedure is that it requires that circulation of resid be stopped => Requires comparison of the time required to accomplish this procedure with the other two options presented MJ Moloney - ExxonMobil April-2010 coking.com 9

Short-Run Drum - Extended Steaming Advantage - Can Cool Resid without Circulating Train Disadvantage - Can result in a mess to handle or clean up => May be only option in multi-train cokers (1) Inject little steam 1-½ hours (2) Switch drum from combo tower to BD; big steam @ 15 klb/hr for 12 hours (3) Block steam; start water flow at max rate limited by pressure; fill to 18-ft probe (4) Shut water, monitor probe; if mid-probe falls, refill with water. Repeat until mid probe holds water level MJ Moloney - ExxonMobil April-2010 coking.com 10

Short-Run Drum - Extended Steaming (cont d) (5) After overhead temp is < 200 F for 1 hour, open drum drain and monitor probe (6) If drum will not drain, refer to Safe Coke Drum Draining, which include blowing back the feed line with steam and pressure draining. Other more drastic measures to consider: => Open top head => Have pit cleaned out and water in pit A Drill through tarry coke with bit in pilot mode B Pump out water with submersible pump attached to drill stem C Drop bottom head and drain water to deck and pit MJ Moloney - ExxonMobil April-2010 coking.com 11

Low Coking Temperatures - Logic Flow Scenarios => How to handle coke drums that have experienced less-than-desired coke drum temperatures There are three basic scenarios to consider: (1) Low coke drum temperatures due to train recirculation (2) Reduced coke drum inlet temperature while feeding resid (3) Reduced coke drum outlet temperature while feeding resid MJ Moloney - ExxonMobil April-2010 coking.com 12

may-2004: Low Coke Drum Temperature attributed to quench water leaking into feed line during coking operations MJ Moloney - ExxonMobil April-2010 coking.com 13

Creating a Mess (2005): Cause of Low Temperature Unknown MJ Moloney - ExxonMobil April-2010 coking.com 14

Scenario (1) Controlled Coke Drum Train Circulation The keys are as follows: (1) Completely displace the resid in the feed line (from the switch valve outlet into the coke drum) with steam (6-10 klb/hr is a good rate) (2) Maintain stripping steam (at least 8 klb/hr) into the coke bed, until a decision is made on how to proceed. => The stripping steam will maintain flow channels in the coke bed and keep temperature at ~400 F minimum. MJ Moloney - ExxonMobil April-2010 coking.com 15

s Scenarios (2 & 3) Low Coke Drum Inlet and/or Outlet Temperature(s) => A more dangerous situation is when the coke drum suffers an extended period of low coke drum temperature while feeding resid. Both the inlet and outlet temperatures of the coke drum MUST be considered Possible causes of a low inlet temperature are: - feed pump trip - unstable feed pumping - fuel gas trip(s) - heater instrumentation problems - leaking quench water into feed line MJ Moloney - ExxonMobil April-2010 coking.com 16

s Scenarios (2 & 3) Low Coke Drum Inlet and/or Outlet Temperature(s) Possible causes of a low outlet temperature are: - Leakage of water from a leaking cutting water line onto top head - Leakage of cold quench oil into the coke drum These basic points should be considered: - Uncoked resid in the drum can cause + high foaming + poor quenching + dangers when deheading - More coke will be made during the period of reduced COT or DOT MJ Moloney - ExxonMobil April-2010 coking.com 17

s February 2010 Scenario: Four-drum coker suffers failure of their Hahn&Clay Force Actuator Bladder: - Requires train circulation to perform repairs - 17:15 Day shift began lowering Train-1 COTs in preparation for recirculation Train-2 on-line spall was not complete at time (2 of 4 passes) - 18:00 Night shift postponed feed out to avoid running the Main Frac at 25% of rate - 18:45 Train-2 spall completed and oil reintroduced to cell 2-19:45 Train-1 placed in recirculation, 2.5 hours after beginning to lower the COTs. Coke drum inlet temperature had dropped to 640 F. MJ Moloney - ExxonMobil April-2010 coking.com 18

s February 2010 Scenario (cont d): Timeline of Events: Oil reintroduced to F602 Cell 2 Attempt to add quenc Quench steam drying out F-601 COTs reduced to prepare for recirculation Steam out Attempt to reintroduce F-601 recirculation begins MJ Moloney - ExxonMobil April-2010 coking.com 19

s February 2010 Scenario (cont d): - Quench steam was immediately introduced to D-603 after switching to recirculation. => Steam ramped to 35 klb/hr and maintained for 2 hours. - Upon completion of steam quenching, the operator attempted to water quench the drum two times, but was unsuccessful. - The operator then attempted to reintroduce steam to the drum, but was unable to establish significant flow. MJ Moloney - ExxonMobil April-2010 coking.com 20

s February 2010 Scenario (cont d): - Key Learning: It is important for operations teams to have an understanding of the difference between feeding cracking resid at 920F and hot tar at 700F. => At >900 F, furnace effluent flow is a turbulent two-phase mixture traveling at 100 ft/s consisting of 80-85 vol% light vapor with the balance being entrained cracking tar droplets. Once this material enters the coke bed, it travels up through the coke bed channels at high velocity to the top of the coke bed. => When the furnace COT is below 740F, the only vapor present is process steam from the furnace and any steam-purged valves. In that case, the flow is predominantly tar traveling at a much lower velocity (~ 5 ft/s). At those conditions, the tar will deposit in the feed line and coke bed channels (previously the high velocities sheared the tar and prevented deposition). The results will be difficulty in cooling and draining the coke bed, as observed in this case. MJ Moloney - ExxonMobil April-2010 coking.com 21

s Scenarios (2 & 3) Low Coke Drum Inlet and/or Outlet Temperature(s) => It is important to assess how much the COT has dropped versus a recommended minimum of 900 F => Determine if there are changes in other factors that may worsen or improve the situation: + feed quality + resid cut point + operating pressure + natural recycle % + distillate recycle % MJ Moloney - ExxonMobil April-2010 coking.com 22

s February 2010 Scenario (cont d): - Starting and stopping steam flow eventually opened a small passageway - Steam flow was maintained and water introduced simultaneously - Steam was removed and the drum was slowly cooled for about a day - Draining was very slow and then stopped - A pressure drain technique was used that actually resulted in expulsion of the soft tar plug from the drain line - Draining then proceeded normally - Special precautions were taken during deheading, which occurred without t incident id - Cutting was normal as well MJ Moloney - ExxonMobil April-2010 coking.com 23