BP SIT Testing Franks Facility Lafayette

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BP SIT Testing Franks Facility Lafayette General Information Status: Franks test well Lafayette La. Rig: Franks Test Rig Casing: 13 3/8, 0 to 4,600 Workstring: 4 ½ IF Brine: Fresh Water Directional: Straight Hole PBTD: 4,600 MD Job Information Date: April 6, 2009 Determine MAP Tool integrity Located MAP Tool outer sleeve in Hydril Slacked off until MAP TOOL unlatched (20,000 k lbs) Summary of Operations With the Hydril closed begin rotating at 30 rpms for 2 hours Beginning pumping at 10 bpm Reciprocate pipe at 60 feet per minute Re-latch MAP TOOL and record over-pull of 40,000 k lbs Unlatch MAP TOOL and bring rpms to 60 for 4 hours No increased torque or drag was noted during the operation 1,100 psi differential pressure was recorded during the test against the lower seal package Increase rotational speed to 70 rpms for 2 hours The MAP TOOL was latched and re-latched 18 times during the 8 hour period Open annular, pull MAP TOOL to surface, wash down MAP TOOL, record visual condition Return MAP TOOL to shop for teardown and TH Hill inspection All seals and bearing were inspected for wear and none was noticed The internal Sea Blue lubricant was tested for possible water invasion and none was recorded

Case History: BP Thunder Horse MC 778-2 Completion (PDQ) SIT 778-2 New Status: Well suspended since December 2008 with inhibited CaBr2 in hole Rig: PDQ Casing: 21 (19.75 ID) marine riser / 18-3/4 BOP 0 to 6,142 11-3/4 102 ppf (10.030 ID) casing 6,142 to 10,587 9-7/8 68 ppf (8.519 ID) casing 10,587 to 23,148 Workstring: 5-7/8 33.53 ppf S-135 CTM57 (7.0 x 4.25 ) 5-7/8 23.40 ppf Z-140 CTM57 (7.0 x 4.25 ) Brine: 12.6 ppg CaBr2 Directional: 30 with KOP at 11,700 and holds angle to TD PBTD: 23,000 MD Date: June 20, 2009 Dirty brine in the hole when MAP tool picked up Tagged fill at 22,972 Located & engaged MAP tool to wash and ream to PBTD with annular closed (taking returns up the choke and kill lines) Washed / reamed to 23,000 PBTD Circulation: 15 bpm at 3,045 psi Rotation: 70 rpms with 26k ft-lbs torque Estimated 8 hours extra C&C time due to filtration unit plugging resulting in reduced filtration rates Rotated for a total of 23 hours Performed MAP tool qualification Tested seals to 4,500 psi

Case History: Newfield Exploration G/B 293 Completion Ocean Victory Rig: Ocean Victory Status: Drill and complete Casing: 21 (19.625 ID) marine riser / 0 to 2,095 18-3/4 BOP 9-7/8 68 ppf (8.519 ID) casing 0 to 21,675 Workstring: 5-7/8 33.53 ppf S-135 XTM-57 (7.125 x 5.135 ) Brine: 13.3 ppg CaBr 2 Mud: 14.9 SBM Directional: 9 Shape PBTD: 21,675 MD Date: June 10, 2010 14.9 SBM displaced with 13.3 CABR2 Located & engaged MAP tool required 5 minutes and began circulating (circulating the long way displacing riser first) Rotated / Reciprocate for 5 hours with 22 ft of stroke Circulate @ 15 bpm at 2,000psi 2,000 psi. Average pressure and 6,200 max psi Rotations 50 rpms average and 56 rpms max Wt to unlatch Map Tool 20K and 30K to re-latch Workstring torque at beginning of rotation was 9K and never went above 10 K 15K wt gained locating to top stop Map Tool was reciprocated at 2 FPM 15 Barrel interface and cleaned up in 1 ½ circulations Map Tool housing had 0 damage and mandrel had only minor scratches which were scotch brite off

Nexen West Delta 45 Well H-15 General Information Status: Workover Rig: Ensco 99 Casing: 9 5/8 43.5# (0 6,082) Liner 7 23# S-95 (6,082 8,110) Workstring: 4 14# IF Brine: 8.5 ppg KCL Mud 11.0 HyCal Directional: 14.1 degrees PBTD: 8,110 MD Job Information Date: Octoiber 6, 2010 Determine MAP Tool integrity for single trip frac systems Max. differential pressure on seals 2,000 psi The MAP TOOL was stroked approximately 40 times Max differential pressure on seals while stroking 600 psi 74 ft of stroke and 63 ft was needed to complete job Summary of Operations Rig up OES non--makering tubular services and mandrel elevators Latch elevators around handling pup and tail in with crane Spin up as per OES and torque bottom pup to recommended torque with iron ruffneck Pull inner bushings and lower housing below rotary 5 in from the top stop Installed inner bushings, continue to 5 in the hole and latch elevators around bottleneck Remove xo and handling pup and bring mandrel #2 into V-door Latch elevators around handling pup and tail in with crane Spin/up and Make-up with OES non-marking tongs, RIH and continue to 5 in the hole At 30 ft. in from the top stop close the bag to 500-800- psi P/U and bump to stop and open bag P/U 3.83 and close bag to 500-800 psi and P/U 1.09 and bump the bottom stop Close bag to closing pressure and RIH and latch elevator around mandrel bottle neck Break out xo and handling pup and bring mandrel #3 into V-door Latch elevators around handling pup and tail in with crane, make up with OES RIH and latch elevators around mandrel bottleneck and break out handling pup Make-up 15 pup to frac head and commence frac operations as per Nexens orders

Case History: Mariner Energy G/C 490 Well # 1 Completion Ocean Victory Rig: Ocean Victory Status: T & A Casing: 21 (19.625 ID) marine riser / 0 to 3,779 18-3/4 BOP 9-5/8 53.50 ppf (8.535 ID) casing 0 to 12,686 Workstring: 5 S-135 19.3 ppf 4.5 IF connection Brine: 12.3 ppg CaBr 2 Mud: 14.2 SBM Directional: Vertical PBTD: 21,675 MD Date: October 10, 2010 14.2 SBM displaced with 12.3 CABR2 Tagged fill @ 78 feet high and washed down to bottom Located & engaged MAP tool pressured up to 2,000 psi. Then pressured to 4,500 psi to test casing. Rotated / Reciprocate for 15 hours with 22 ft of stroke Circulate @ 13.5 bpm at 3,000 4,000 psi 2,000 psi. Average pressure and 4,100 max psi Rotations 30 rpms average and 56 rpms max Difference in open bag torque versus closed bag torque was less than 500 ft/lbs. Initial NTU reading was 150 15 bbl interface on the casing and a 35 bbl interface on the riser and cleaned up in 1 ½ circulations Map Tool housing had 0 damage and mandrel had only minor scratches which were scotch brite off

Case History: ERT G/C 238 Well ST3BP1 Completion Ocean Victory Rig: Ocean Victory Status: T & A Casing: 21 (19.75 ID) marine riser / 0 to 2,418 18-3/4 BOP 9-5/8 53.50 ppf Q-125 (8.379 ID) casing 0 to 16,730 Workstring: 5. S-135 19.5 ppf 4.5 IF connection Brine: 14.2 ppg CaBr 2 Mud: 14.3 SBM Directional: 49 degrees PBTD: 16,645 MD Date: April 21, 2011 14.3 SBM displaced with 14.2 CABR2 Used the Map Tool in conjunction with RTTS for 2 hour negative shoe track test Rotated and reciprocated 36 hours while cleaning pits Rotated / Reciprocate for 11 hours with 42 ft of stroke while displacing Circulate @ 20 bpm/riser and 15 bpm/casing 2,800 psi. average pressure and 5,000 max psi Rotations 50 rpms average and 55 rpms max Spotted MAP TOOL in 15 foot seas Due to the heaving action of the rig the annular would have been damaged even with the motion compensator without the MAP TOOL Initial NTU reading was 350 which cleaned up to 150 after one circulation and 25 NTU s after short trip and 1 ½ circulations (note initial high NTU reading was due to filter presses shutting down during displacement which cased the displacement to shut down twice) 25 bbl interface on the casing and a 25 bbl Interface on the riser Used a new sling system incorporating a pulley system