EP WELLS DAILY OPERATIONS REPORT Report 29 04/21/2017

Size: px
Start display at page:

Download "EP WELLS DAILY OPERATIONS REPORT Report 29 04/21/2017"

Transcription

1 4/22/217 8:23:32 Report Version: R9 Generated from data in EDM/Opens/PROFILE 1 RESTRICTED Report 29 4/21/217 Company Type bore WBS No/API No PERMIAN Development / Event Summary Event Type Drilling only Event Start Date 11/21/216 Days on Location 28.5 Objective Drill - Wolfcamp HZ Original Spud Date 11/21/216 Days Since Spud Est. Days 2. Contractor PRECISION Work Unit PRECISION 559 Days To Release Rig Phone/FAX No. Status Supervisor DENNIS MORGAN Measured Depth 15,814. Engineer YERMEK TYNYSHBAYEV TVD 11,73.62 Other Supervisor TANNER MANUEL, YU LIU 24 Hr Progress Depth Ref/Grd Elev/Water Depth DFE: 2,882.3 / 2,856.3 Hole size THF Datum Daily (hr/%) 2.5/1.42 Days Ahd(-) Bhnd(+)(5/5) Actual cost to date/afe 2,332,628/2,75, Last Casing MD 7.in@11,95.ft Next Casing MD 4.5in@18,2.ft Current MW / BH EMW(ppg) 13.6/ Actual divided by AFE Daily Cost.85 41,252 LOT/FIT EMW(ppg) Lithology Formation/MD Top Last Incident HSE Summary Date Days Last Incident Date Days KPI's LWC RWC MTC FAC Last casing pressure test PSI NII HPI GOAL ZERO DAYS PS BARRIER EVENT PS barrier bowtie review 8/24/ TRCF LWCF Safety Cards - Safe Safety Card - Unsafe SSE% Last casing pressure(psi) Safety Comments: MAN HRS: 286 HSE Drills Drills/Tests Date Days Since Last Last Derrick Inspection Last BOP function test Last BOP Test Next BOP Test 4/17/217 4/17/217 5/8/ JSA's/Toolbox Talks Days Since Last Drill Hour Summary Operations Summary TIH W/ LATERAL BHA F/ 1363' - T/ 14534'. WASH & REAM F/ 14534' - T/ PUMP SWEEP. ROT DRILL F/ 15814' - T/ 15838'. PUMP SWEEP. ROTATE & SLIDE F/ 15838' - T/ 16225'. Update Since Report Time ROTATE & SLIDE F/ 16225' - T/ 16481'. 24 Hour Forecast CONTINUE DRILLING LATERAL. (TD 1843'). PUMP SWEEPS. POOH TO RUN LINER.

2 4/22/217 8:23:32 Report Version: R9 Generated from data in EDM/Opens/PROFILE 2 RESTRICTED bore Report 29 4/21/217 Time Summary Start Hours PH OPN Detail Drilled Depth level Rig Rate Description : 1.5 MNH1 TIH 15,814. TIH F/ T/ 14534'. HIT TIGHT SPOT. 1:3 6: 9: 4.5 MNH1 TIH 15, MNH1 CDM 15, MNH1 TIH 15,814. WASH & REAM F/ 14534' - T/ 15229'. WORKING THROUGH TIGHTS SPOTS. 3 GPM, 7 RPM CIRCULATE BTMS UP DUE TO 4K DRAG & EXCESS TORQUE. 3 GPM, 1 RPM DOWN, 5 RPM UP, WORKING FULL STAND. WASH & REAM F/ 15229' - T/ 15814' (BOTTOM). 3 GPM, 7 RPM. 11:3 12: 13:3.5 MNH1 DRL 15, MNH1 CDM 15, MNH1 SVC 15,838. ROTATE DRILL F/ 15814' T/ 15838' 48 FPH) WOB: 34K RPM: SURF 8 MOTOR 215 BIT 295 PRESSURE: 5591 PSI FLOW: 268 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 178K S/O: 147K ROT: 157K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 CIRCULATE BTMS UP 3 GPM, 1 RPM DOWN, 5 RPM UP, WORKING FULL STAND. SERVICE : SERVICE TOP DRIVE 14: 14:3.5 MNH1 DRL 15, MNH1 DRL 15, ROTATE DRILL F/ 15838' T/ 15853' 3 FPH) WOB: 34K RPM: SURF 8 MOTOR 215 BIT 295 PRESSURE: 5591 PSI FLOW: 268 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 178K S/O: 147K ROT: 157K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 : TROUBLESHOOT TOP DRIVE. 17: 19: 2: 21: 2. MNH1 DRL 15, MNH1 DRL 15, MNH1 DRL 15, MNH1 DRL 15,968. SLIDE DRILL F/ 15853' T/ 1595' 26 FPH) WOB: 3 K RPM:MOTOR 24 BIT 24 PRESSURE: 5591 PSI FLOW: 3 GPM TORQUE: ON BTM 8 K P/U: 18K S/O: 14K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 ROTATE DRILL F/ 1595' T/ 15946' 41 FPH) WOB: 22K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 63 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 18K S/O: 14K ROT: 155K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 SLIDE DRILL F/ 15946' T/ 15968' 22 FPH) WOB: 3 K RPM:MOTOR 24 BIT 24 PRESSURE: 63 PSI FLOW: 3 GPM TORQUE: ON BTM 8 K P/U: 18K S/O: 14K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 ROTATE DRILL F/ 15968' T/ 1627' 12 FPH) WOB: 31K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 65 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 18K S/O: 14K ROT: 155K B/G GAS: 173 UNITS B/U GAS: 27 UNITS

3 4/22/217 8:23:32 Report Version: R9 Generated from data in EDM/Opens/PROFILE 3 RESTRICTED bore Report 29 4/21/217 Time Summary Start Hours PH OPN Detail Drilled Depth level Rig Rate Description MW: 13.6 MOTOR REV/GAL:.8 23: 1. MNH1 DRL 15,968. SLIDE DRILL F/ 1627' T/ 16225' 18 FPH) WOB: 3 K RPM:MOTOR 24 BIT 24 PRESSURE: 63 PSI FLOW: 3 GPM TORQUE: ON BTM 8 K P/U: 18K S/O: 14K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 Total 24. Summary Start Date/Time Responsible Company Code Failure MD Ops Code Type* Equipment Type Net time (hr) Gross time (hr) Severity Status 4/21/217 14:3 PRECISION Rig/Work DRILLING Unit Misc COMPANY LP 15,853. DRL N OPEN Description: TROUBLESHOOT TOP DRIVE. Title: TROUBLESHOOT TOP DRIVE. Total MD Inc. Azi. TVD N/S Deepest 5 Surveys E/W V.Sec DLeg ( /1ft) 15, , , , PTW MWD_216 15, , , , PTW MWD_216 15, , , , PTW MWD+HDGM+AXIAL_216 15, , , , PTW MWD+HDGM_216 15, , , , PTW MWD+HDGM_216 Fluid Details Mud type Invermul Oil/Water (%) 56.5/16. POM (cc) MD 15,826. TS/HGS/LGS (%) 25.7/18./7.7 CaCl2 (%) Mud Density (ppg) 13.6 Sand (%) Caom/Clom (ppm) Vis (s/qt) 74. Oil/Water Ratio (%) 77.9/22.1 ACT PV/YP (cp/lbf/1ft²) 34./15. XS Lime(lbm/bbl) 2.85 Gels 1 s/m (lbf/1ft²) 9./14. LCM (lbm/bbl) ES (Volts) 446. API/HTHP WL (cc/3min) /1. ECD (ppg) R6/3 FC/HTHP FC (32nd") /4. H2S (gas unit) R2/1 WPS (ppm) 264,729 KCl (%) R6/3 FL temp. ( F) Ditch Magnet in Last 24hrs/Cum. (gm) Bit Details Bit no. Size Manufacturer Model no. Class IADC Serial Size MD in MD out IADC Dull Grade code no. (32nd") ULTERRA U513S x16 15, Tool

4 4/22/217 8:23:32 Report Version: R9 Generated from data in EDM/Opens/PROFILE 4 RESTRICTED bore Report 29 4/21/217 MD 15, , ,95. 15, , ,27. 16,225. WOB Min/Max Current RPM (rpm) Flow rate (gpm) SPP (psi) P bit (psi) Bit Operations Bit HHP (hp) Hours (hr) Footage ROP (ft/hr) Hours cum (hr) Footage cum. 34./ , / , / , / , / , / , / , ROP cum. (ft/hr) Item description 4" DP 5" NOV SHOCK SUB 4" DP 5" NOV AGITATOR SHOCK SUB COMBO 4" DP DOG LEG REAMER 4" DP X/O FLOAT SUB FILTER SUB NMSC GAP SUB ASSY VELOCITY 475 CENT COLLAR ASSY VELOCITY 475 LANDING SUB ASSY VELOCITY 475 X/O SUB VELOCITY NMPC # Jts Length Drillstring Components OD Max OD ID Connection Name Weight (ppf) Grade Serial no. 1 11, XT XT , XT XT-39 W / SHTL , XT XT-39 B1/A XT XT-39 DR /2 IF NESFS /2 IF DR /2 IF DR /2 IF VG47574P TS ACME VC ACME VL /2 IF VX /2 IF DR31745 MUD MOTOR 5 NOV 513 BIT #11 RUN # " ULTERRA U513S (5X16's) SN: /2 IF 24XH PTS /2 IF Drillstring Details Date/Time in Date/Time out BHA no. BHA Length Min. ID Purpose 4/2/217 8: DRILL 6.125" PRODUCTION HOLE SECTION MD 15,838. SW Up 178. SW Down 147. SW Rotn 157. Drag 21. Tq On Btm (ft-lbf) 13,. Tq Off Btm (ft-lbf) 8,. Footage , ,95. 15, , ,27. 16, ,. 8, ,. 8, ,. 8,

5 4/22/217 8:23:32 Report Version: R9 Generated from data in EDM/Opens/PROFILE 5 RESTRICTED bore Report 29 4/21/217 DIESEL ON LOCATION: 9256 GAL DIESEL DELIVERED: GAL DIESEL USED: 279 LNG USED: 3.66 GAL Remarks

6 4/23/217 5:29:36 Report Version: R9 Generated from data in EDM/Opens/PROFILE 1 RESTRICTED Report 3 4/22/217 Company Type bore WBS No/API No PERMIAN Development / Event Summary Event Type Drilling only Event Start Date 11/21/216 Days on Location 29.5 Objective Drill - Wolfcamp HZ Original Spud Date 11/21/216 Days Since Spud Est. Days 2. Contractor PRECISION Work Unit PRECISION 559 Days To Release Rig Phone/FAX No. Status Supervisor DENNIS MORGAN Measured Depth 15,814. Engineer YERMEK TYNYSHBAYEV TVD 11,73.62 Other Supervisor TANNER MANUEL, YU LIU 24 Hr Progress Depth Ref/Grd Elev/Water Depth DFE: 2,882.3 / 2,856.3 Hole size THF Datum Daily (hr/%) / Days Ahd(-) Bhnd(+)(5/5) Actual cost to date/afe 2,378,565/2,75, Last Casing MD 7.in@11,95.ft Next Casing MD 4.5in@18,2.ft Current MW / BH EMW(ppg) / Actual divided by AFE Daily Cost.86 45,937 LOT/FIT EMW(ppg) Lithology Formation/MD Top Last Incident HSE Summary Date Days Last Incident Date Days KPI's LWC RWC MTC FAC Last casing pressure test PSI NII HPI GOAL ZERO DAYS PS BARRIER EVENT PS barrier bowtie review 8/24/ TRCF LWCF Safety Cards - Safe Safety Card - Unsafe SSE% Last casing pressure(psi) Safety Comments: MAN HOURS - 274HRS HSE Drills Drills/Tests Date Days Since Last Last Derrick Inspection Last BOP function test Last BOP Test Next BOP Test 4/17/217 4/17/217 5/8/ JSA's/Toolbox Talks Days Since Last Drill Hour Summary ROTATE & SLIDE F/16,225' T/17,667' Update Since Report Time ROTATE & SLIDE F/17,667' T/17992' 24 Hour Forecast Operations Summary DRILL TO TD (18,43'), PUMP CLEANUP CYCLES, POOH L/D DP, DROP SHOE, CONT POOH RACKING BACK DP TO RUN LINER, M/U CASING TOOL, RUN 4.5'' LINER.

7 4/23/217 5:29:36 Report Version: R9 Generated from data in EDM/Opens/PROFILE 2 RESTRICTED bore Report 3 4/22/217 Time Summary Start Hours PH OPN Detail Drilled Depth level Rig Rate Description : 1. MNH1 DRL 16,247. SLIDE DRILL F/ 16225' T/ 16247' 22 FPH) WOB: 3 K RPM: MOTOR 24 BIT 24 PRESSURE: 63 PSI FLOW: 3 GPM TORQUE: ON BTM 8 K P/U:25K S/O:1K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 1: 2.5 MNH1 DRL 16,48. ROTATE DRILL F/ 16247' T/ 1648' 93 FPH) WOB: 31K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 65 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 25K S/O: 1K ROT: 17K B/G GAS: 173 UNITS B/U GAS: 27 UNITS MW: 13.6 MOTOR REV/GAL:.8 3:3 1.5 MNH1 DRL 16,518. SLIDE DRILL F/ 1648' T/ 16518' 25 FPH) WOB: 3 K RPM: MOTOR 24 BIT 24 PRESSURE: 63 PSI FLOW: 3 GPM TORQUE: ON BTM 8 K P/U:25K S/O:1K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 5:.5 MNH1 DRL 16,557. ROTATE DRILL F/ 16518' T/ 16557' 78 FPH) WOB: 31K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 65 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 25K S/O: 1K ROT: 17K B/G GAS: 173 UNITS B/U GAS: 27 UNITS MW: 13.6 MOTOR REV/GAL:.8 5:3.5 MNH1 SVC 16,557. SERVICE: SERVICE TOP DRIVE 6: 6:3 8:3.5 MNH1 DRL 16, MNH1 DRL 16, MNH1 DRL 16,842. ROTATE DRILL F/ 16557' T/ 16572' 3 FPH) WOB: 31K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 65 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 25K S/O: 1K ROT: 17K B/G GAS: 173 UNITS B/U GAS: 27 UNITS MW: 13.6 MOTOR REV/GAL:.8 SLIDE DRILL F/ 16572' T/ 16622' 25 FPH) WOB: 3 K RPM: MOTOR 24 BIT 24 PRESSURE: 63 PSI FLOW: 3 GPM TORQUE: ON BTM 8 K P/U:19K S/O:138K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 ROTATE DRILL F/ 16622' T/ 16842' 147 FPH) WOB: 34K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 65 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 25K S/O: 1K ROT: 17K B/G GAS: 173 UNITS B/U GAS: 27 UNITS MW: 13.6 MOTOR REV/GAL:.8

8 4/23/217 5:29:36 Report Version: R9 Generated from data in EDM/Opens/PROFILE 3 RESTRICTED bore Report 3 4/22/217 Time Summary Start Hours PH OPN Detail Drilled Depth level Rig Rate Description 1: 2. MNH1 DRL 16,872. SLIDE DRILL F/ 16842' T/ 16872' 15 FPH) WOB: 3 K RPM: MOTOR 24 BIT 24 PRESSURE: 63 PSI FLOW: 3 GPM TORQUE: ON BTM 8 K P/U:19K S/O:138K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 12:.5 MNH1 DRL 16,931. ROTATE DRILL F/ T/ FPH) WOB: 34K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 65 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 25K S/O: 1K ROT: 17K B/G GAS: 173 UNITS B/U GAS: 27 UNITS MW: 13.6 MOTOR REV/GAL:.8 12:3 2. MNH1 DRL 16,971. SLIDE DRILL F/ T/ FPH) WOB: 3 K RPM: MOTOR 24 BIT 24 PRESSURE: 63 PSI FLOW: 3 GPM TORQUE: ON BTM 8 K P/U:19K S/O:138K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 14:3 2. MNH1 DRL 17,143. ROTATE DRILL F/ T/ FPH) WOB: 34K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 65 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 25K S/O: 1K ROT: 17K B/G GAS: 173 UNITS B/U GAS: 27 UNITS MW: 13.6 MOTOR REV/GAL:.8 16:3.5 MNH1 SVC 17,143. SERVICE: SERVICE TOP DRIVE 17: 18: 19:3 21:3 1. MNH1 DRL 17, MNH1 DRL 17, MNH1 DRL 17, MNH1 DRL 17,431. ROTATE DRILL F/ T/ FPH) WOB: 34K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 65 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 25K S/O: 12K ROT: 17K B/G GAS: 173 UNITS B/U GAS: 27 UNITS MW: 13.6 MOTOR REV/GAL:.8 ROTATE DRILL F/ 1723 T/ FPH) WOB: 34K RPM: SURF 8 MOTOR 232 BIT 312 PRESSURE: 65 PSI FLOW: 29 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 25K S/O: 12K ROT: 17K B/G GAS: 173 UNITS B/U GAS: 27 UNITS MW: 13.6 MOTOR REV/GAL:.8 SLIDE DRILL F/ 1738 T/ FPH) WOB: 33 K RPM: MOTOR 224 BIT 224 PRESSURE: 497 PSI FLOW: 28 GPM TORQUE: ON BTM 8 K P/U:23K S/O:12K B/G GAS: 1 UNITS B/U GAS: 25 UNITS MW: 13.6 MOTOR REV/GAL:.8 ROTATE DRILL F/ T/ FPH) WOB: 25-3K

9 4/23/217 5:29:36 Report Version: R9 Generated from data in EDM/Opens/PROFILE 4 RESTRICTED bore Report 3 4/22/217 Time Summary Start Hours PH OPN Detail Drilled Depth level Rig Rate Description RPM: SURF 8 MOTOR 224 BIT 34 PRESSURE: 65 PSI FLOW: 28 GPM TORQUE: ON BTM 13 K OFF BTM 8 K P/U: 25K S/O: 12K ROT: 17K B/G GAS: 173 UNITS B/U GAS: 27 UNITS MW: 13.6 MOTOR REV/GAL:.8 Total 24. MD Inc. Azi. TVD N/S Deepest 5 Surveys E/W V.Sec DLeg ( /1ft) 15, , , , PTW MWD_216 15, , , , PTW MWD_216 15, , , , PTW MWD+HDGM+AXIAL_216 15, , , , PTW MWD+HDGM_216 15, , , , PTW MWD+HDGM_216 Fluid Details Mud type Invermul Oil/Water (%) POM (cc) MD TS/HGS/LGS (%) CaCl2 (%) Mud Density (ppg) Sand (%) Caom/Clom (ppm) Vis (s/qt) Oil/Water Ratio (%) ACT PV/YP (cp/lbf/1ft²) XS Lime(lbm/bbl) Gels 1 s/m (lbf/1ft²) LCM (lbm/bbl) ES (Volts) API/HTHP WL (cc/3min) ECD (ppg) R6/3 FC/HTHP FC (32nd") H2S (gas unit) R2/1 WPS (ppm) KCl (%) R6/3 FL temp. ( F) Ditch Magnet in Last 24hrs/Cum. (gm) Bit Details Bit no. Size Manufacturer Model no. Class IADC Serial Size MD in MD out IADC Dull Grade code no. (32nd") ULTERRA U513S x16 15, Tool Bit Operations MD WOB Min/Max Current RPM (rpm) Flow rate (gpm) SPP (psi) P bit (psi) Bit HHP (hp) Hours (hr) Footage ROP (ft/hr) Hours cum (hr) Footage cum. ROP cum. (ft/hr) Item description 4" DP 5" NOV SHOCK SUB 4" DP 5" NOV AGITATOR SHOCK SUB COMBO 4" DP DOG LEG REAMER 4" DP X/O # Jts Length Drillstring Components OD Max OD ID Connection Name Weight (ppf) Grade Serial no. 1 11, XT XT , XT XT-39 W / SHTL , XT XT-39 B1/A XT XT-39 DR28529

10 4/23/217 5:29:36 Report Version: R9 Generated from data in EDM/Opens/PROFILE 5 RESTRICTED bore Report 3 4/22/217 Item description FLOAT SUB FILTER SUB NMSC GAP SUB ASSY VELOCITY 475 CENT COLLAR ASSY VELOCITY 475 LANDING SUB ASSY VELOCITY 475 X/O SUB VELOCITY NMPC # Jts Length Drillstring Components OD Max OD ID Connection Name Weight (ppf) Grade Serial no /2 IF NESFS /2 IF DR /2 IF DR /2 IF VG47574P TS ACME VC ACME VL /2 IF VX /2 IF DR31745 MUD MOTOR 5 NOV 513 BIT #11 RUN # " ULTERRA U513S (5X16's) SN: /2 IF 24XH PTS /2 IF Drillstring Details Date/Time in Date/Time out BHA no. BHA Length Min. ID Purpose 4/2/217 8: DRILL 6.125" PRODUCTION HOLE SECTION DIESEL ON LOCATION: 4826 GAL DIESEL DELIVERED: GAL DIESEL USED: 443 LNG USED: 272 GAL NOTIFIED TRRC OF LINER RUN & CEMENT: OPERATOR #9 CARLA Remarks

11 4/25/217 5:54:34 Report Version: R9 Generated from data in EDM/Opens/PROFILE 1 RESTRICTED Report 32 4/24/217 Company Type bore WBS No/API No PERMIAN Development / Event Summary Event Type Drilling only Event Start Date 11/21/216 Days on Location 31.5 Objective Drill - Wolfcamp HZ Original Spud Date 11/21/216 Days Since Spud Est. Days 2. Contractor PRECISION Work Unit PRECISION 559 Days To Release Rig Phone/FAX No. Status Supervisor DENNIS MORGAN Measured Depth 18,737. Engineer YERMEK TYNYSHBAYEV TVD 11,776.5 Other Supervisor TANNER MANUEL, YU LIU 24 Hr Progress Depth Ref/Grd Elev/Water Depth DFE: 2,882.3 / 2,856.3 Hole size THF Datum Daily (hr/%) / Days Ahd(-) Bhnd(+)(5/5) Actual cost to date/afe 2,583,135/2,75, Last Casing MD 7.in@11,95.ft Next Casing MD 4.5in@18,2.ft Current MW / BH EMW(ppg) / Actual divided by AFE Daily Cost.94 1,756 LOT/FIT EMW(ppg) Lithology Formation/MD Top Last Incident HSE Summary Date Days Last Incident Date Days KPI's LWC RWC MTC FAC Last casing pressure test PSI NII HPI GOAL ZERO DAYS PS BARRIER EVENT PS barrier bowtie review 8/24/ TRCF LWCF Safety Cards - Safe Safety Card - Unsafe SSE% Last casing pressure(psi) Safety Comments: MAN HRS: 384 HSE Drills Drills/Tests Date Days Since Last Last Derrick Inspection Last BOP function test Last BOP Test Next BOP Test 4/17/217 4/17/217 5/8/ JSA's/Toolbox Talks Days Since Last Drill Hour Summary Operations Summary L/D BHA. RUN 4.5" LINER T/ 7,492'. BREAK CIRCULATION. RUN 4.5" LINER TO 18737' W/ 4" DP. INSTALL CEMENT HEAD. DROP 1.5" BALL. SET PACKER. CEMENT WELL. Update Since Report Time DISPLACE WELL WITH 13.6 OBM. DISPLACE WELL WITH 1# BRINE HOLDING BOTTOM HOLE PRESSURE THROUGH CHOKES. FLOW CHECK (NO FLOW). 24 Hour Forecast POOH LAYING DOWN DP. L/D DP IN DERRICK. PULL BIT GUIDE INSTALL BPV. CLEAN PITS. PREPARE FOR MOVE.

12 4/25/217 5:54:34 Report Version: R9 Generated from data in EDM/Opens/PROFILE 2 RESTRICTED bore Report 32 4/24/217 Time Summary Start Hours PH OPN Detail Drilled Depth level Rig Rate Description : 1.5 MNH1 TOH 18,737. POOH F/ 1824' - BHA. 1:3 1. MNH1 TOH 18,737. L/D BHA. 2:3.5 MNH1 SVC 18,737. SERVICE: GREASE TOP DRIVE DRAWWORKS, BLOCKS 3: 1. MNH1 RIC 18,737. PJSM W/ CREW AND CASING CREW. R/U CASING CREW. 4: 5.5 MNH1 CLR 18,737. RUN 4.5" LINER F/ SURFACE T/ 7,492'. 11.6# P11 DQX. 9:3.5 MNH1 CLR 18,737. P/U PACKER & CIRCULATE. 1:.5 MNH1 CLR 18,737. R/D CASING CREW. 1:3 6.5 MNH1 CLR 18,737. RUN LINER W/ 4" DP F/ 7,492' - T/ 18737'. 17: 2. MNH1 RCC 18,737. CIRCULATE HOLE CLEAN. 19: 19:3.5 MNH1 RCC 18, MNH1 RCC 18,737. P/U & M/U CEMENT HEAD. INSTALL LO TORQUE. BREAK CIRCULATION. DROP 1.5" BRASS BALL. R/U CEMENT LINES. 21:.5 MNH1 RCC 18,737. PRESSURE UP PACKER T/ 17 PSI. RELEASE. P/U TO VERIFY. 21:3.5 MNH1 RCC 18,737. INSTALL CEMENT LINES TO CEMENT HEAD. 22: 2. MNH1 CEM 18,737. CEMENT 4.5 LINER WITH 5 BBL OF 14 PPG ULTRA FLUSH SPACER, PUMP 1655 SKS OF 14.5 PPG CLASS H PREMIUM CEMENT SLURRY. DROP PLUG. DISPLACE W/ 2 BBLS OF FW, 8 BBLS OF 1. PPG BRINE AND 3 BBL FW AND 18 OBM. BUMP PLUG WITH 5 OVER AND HOLD FLOATS HELD. SET PACKER. TEST CASING T/ 25# HELD FOR 5MIN. GOOD TEST. Total 24. MD Inc. Azi. TVD N/S Deepest 5 Surveys E/W V.Sec DLeg ( /1ft) 17, , , , PTW MWD_216 17, , , , PTW MWD_216 17, , , , PTW MWD_216 17, , , , PTW MWD_216 18, , , , PTW MWD_216 Fluid Details Mud type Invermul Oil/Water (%) POM (cc) MD TS/HGS/LGS (%) CaCl2 (%) Mud Density (ppg) Sand (%) Caom/Clom (ppm) Vis (s/qt) Oil/Water Ratio (%) ACT PV/YP (cp/lbf/1ft²) XS Lime(lbm/bbl) Gels 1 s/m (lbf/1ft²) LCM (lbm/bbl) ES (Volts) API/HTHP WL (cc/3min) ECD (ppg) R6/3 FC/HTHP FC (32nd") H2S (gas unit) R2/1 WPS (ppm) KCl (%) R6/3 FL temp. ( F) Ditch Magnet in Last 24hrs/Cum. (gm) Bit Details Bit no. Size Manufacturer Model no. Class IADC Serial Size MD in MD out IADC Dull Grade code no. (32nd") ULTERRA U513S x16 15, Tool

13 4/25/217 5:54:34 Report Version: R9 Generated from data in EDM/Opens/PROFILE 3 RESTRICTED bore Report 32 4/24/217 Bit Operations MD WOB Min/Max Current RPM (rpm) Flow rate (gpm) SPP (psi) P bit (psi) Bit HHP (hp) Hours (hr) Footage ROP (ft/hr) Hours cum (hr) Footage cum. ROP cum. (ft/hr) Item description 4" DP 5" NOV SHOCK SUB 4" DP 5" NOV AGITATOR SHOCK SUB COMBO 4" DP DOG LEG REAMER 4" DP X/O FLOAT SUB FILTER SUB NMSC GAP SUB ASSY VELOCITY 475 CENT COLLAR ASSY VELOCITY 475 LANDING SUB ASSY VELOCITY 475 X/O SUB VELOCITY NMPC # Jts Length Drillstring Components OD Max OD ID Connection Name Weight (ppf) Grade Serial no. 1 14, XT XT , XT XT-39 W / SHTL , XT XT-39 B1/A XT XT-39 DR /2 IF NESFS /2 IF DR /2 IF DR /2 IF VG47574P TS ACME VC ACME VL /2 IF VX /2 IF DR31745 MUD MOTOR 5 NOV 513 BIT #11 RUN # " ULTERRA U513S (5X16's) SN: /2 IF 24XH PTS /2 IF Drillstring Details Date/Time in Date/Time out BHA no. BHA Length Min. ID Purpose 4/2/217 8: DRILL 6.125" PRODUCTION HOLE SECTION DIESEL ON LOCATION: 8623 GAL DIESEL DELIVERED: GAL DIESEL USED: 651 GAL LNG USED: GAL Remarks

14 4/26/217 5:31:17 Report Version: R9 Generated from data in EDM/Opens/PROFILE 1 RESTRICTED Report 33 4/25/217 Company Type bore WBS No/API No PERMIAN Development / Event Summary Event Type Drilling only Event Start Date 11/21/216 Days on Location 32.5 Objective Drill - Wolfcamp HZ Original Spud Date 11/21/216 Days Since Spud Est. Days 2. Contractor PRECISION Work Unit PRECISION 559 Days To Release Rig Phone/FAX No. Status Supervisor DENNIS JOHNSON Measured Depth 18,737. Engineer YERMEK TYNYSHBAYEV TVD 11,776.5 Other Supervisor TANNER MANUEL, YU LIU 24 Hr Progress. Depth Ref/Grd Elev/Water Depth DFE: 2,882.3 / 2,856.3 Hole size THF Datum Daily (hr/%) / Days Ahd(-) Bhnd(+)(5/5) Actual cost to date/afe 2,745,816/2,75, Last Casing MD 7.in@11,95.ft Next Casing MD 4.5in@18,737.ft Current MW / BH EMW(ppg) / Actual divided by AFE Daily Cost 1. 67,324 LOT/FIT EMW(ppg) Lithology Formation/MD Top Last Incident HSE Summary Date Days Last Incident Date Days KPI's LWC RWC MTC FAC Last casing pressure test PSI NII HPI GOAL ZERO DAYS PS BARRIER EVENT PS barrier bowtie review 8/24/ TRCF LWCF Safety Cards - Safe Safety Card - Unsafe SSE% Last casing pressure(psi) Safety Comments: MAN HRS: 378 HSE Drills Drills/Tests Date Days Since Last Last Derrick Inspection Last BOP function test Last BOP Test Next BOP Test 4/17/217 4/17/217 5/8/ JSA's/Toolbox Talks Days Since Last Drill Hour Summary Operations Summary SET PACKER. CIRCULATE OUT EXCESS CEMENT (2 BBL OF CEMENT TO SURFACE). PRESSURE TEST TO 25 PSI HELD FOR 5 MIN (GOOD TEST). DISPLACE WELL W/ 1# BRINE. POOH & L/D DP. Update Since Report Time PULL BIT GUIDE & SET BPV. REMOVE LINES F/ BOPS. FINISH PIT CLEANING. 24 Hour Forecast FINISH N/D BOPS & INSTALL TA CAP. RELEASE. START MOVE.

15 4/26/217 5:31:17 Report Version: R9 Generated from data in EDM/Opens/PROFILE 2 RESTRICTED bore Report 33 4/25/217 Time Summary Start Hours PH OPN Detail Drilled Depth level Rig Rate Description :.5 MNH1 SLP 18,737. SET PACKER. P/U BREAK OVER WEIGHT 25K. SLACK OFF T/ 165K, SLACK OFF T/ 12K. HOLD WEIGHT. MEASURE OUT 25' TO COMPLETE STING OUT. :3 1. MNH1 SLP 18,737. CIRCULATE OUT EXCESS CEMENT W/ 13.6# OBM. 2 BBL OF CEMENT TO SURFACE. 1:3.5 MNH1 SLP 18,737. TEST PACKER. PRESSURE T/ 25 PSI AND HOLD FOR 5 MIN. GOOD TEST. 2: 2.5 MNH1 SLP 18,737. DISPACE WELL F/ 13.6# OBM T/ 1# BRINE. HOLDING BHP CONSTANT THROUGH CHOKES. 4:3.5 MNH1 SLP 18,737. FLOW CHECK. NO FLOW. MONITORING WELL ON TRIP TANK. 5:.5 MNH1 SLP 18,737. L/D CEMENT HEAD. 5:3 16: 1.5 MNH1 TOH 18, MNH1 TOH 18,737. POOH & L/D DP F/ 11233' T/ SURFACE. L/D PACKER RUNNING TOOL. TIH W/ DP. 82 STANDS. 19:3 4.5 MNH1 TOH 18,737. POOH & L/D DP T/ SURFACE. Total 24. MD Inc. Azi. TVD N/S Deepest 5 Surveys E/W V.Sec DLeg ( /1ft) 17, , , , PTW MWD_216 17, , , , PTW MWD_216 17, , , , PTW MWD_216 17, , , , PTW MWD_216 18, , , , PTW MWD_216 Fluid Details Mud type Invermul Oil/Water (%) POM (cc) MD TS/HGS/LGS (%) CaCl2 (%) Mud Density (ppg) Sand (%) Caom/Clom (ppm) Vis (s/qt) Oil/Water Ratio (%) ACT PV/YP (cp/lbf/1ft²) XS Lime(lbm/bbl) Gels 1 s/m (lbf/1ft²) LCM (lbm/bbl) ES (Volts) API/HTHP WL (cc/3min) ECD (ppg) R6/3 FC/HTHP FC (32nd") H2S (gas unit) R2/1 WPS (ppm) KCl (%) R6/3 FL temp. ( F) DIESEL ON LOCATION: 7785 GAL DIESEL DELIVERED: GAL DIESEL USED: 838 GAL LNG USED: GAL Ditch Magnet in Last 24hrs/Cum. (gm) Remarks Tool

16 4/27/217 11:46:9 Report Version: R9 Generated from data in EDM/Opens/PROFILE 1 RESTRICTED Report 34 4/26/217 Company Type bore WBS No/API No PERMIAN Development / Event Summary Event Type Drilling only Event Start Date 11/21/216 Days on Location Objective Drill - Wolfcamp HZ Original Spud Date 11/21/216 Days Since Spud 2. Est. Days 2. Contractor PRECISION Work Unit PRECISION 559 Days To Release Rig Phone/FAX No. Status Supervisor DENNIS JOHNSON Measured Depth 18,737. Engineer YERMEK TYNYSHBAYEV TVD 11,776.5 Other Supervisor TANNER MANUEL, YU LIU 24 Hr Progress Depth Ref/Grd Elev/Water Depth DFE: 2,882.3 / 2,856.3 Hole size THF Datum Daily (hr/%) / Days Ahd(-) Bhnd(+)(5/5) Actual cost to date/afe 2,82,421/2,75, Last Casing MD 7.in@11,95.ft Next Casing MD 4.5in@18,737.ft Current MW / BH EMW(ppg) / Actual divided by AFE Daily Cost ,787 LOT/FIT EMW(ppg) Lithology Formation/MD Top Last Incident HSE Summary Date Days Last Incident Date Days KPI's LWC RWC MTC FAC Last casing pressure test PSI NII HPI GOAL ZERO DAYS PS BARRIER EVENT PS barrier bowtie review 8/24/ TRCF LWCF Safety Cards - Safe Safety Card - Unsafe SSE% Last casing pressure(psi) Safety Comments: HSE Drills Drills/Tests Date Days Since Last Last Derrick Inspection Last BOP function test Last BOP Test Next BOP Test 4/17/217 4/17/217 5/8/ JSA's/Toolbox Talks Days Since Last Drill Hour Summary Operations Summary PULL BIT GUIDE. INSTALL BPV. N/D BOPS. INSTALL DUST CAP. 6. Update Since Report Time 24 Hour Forecast

17 4/27/217 11:46:9 Report Version: R9 Generated from data in EDM/Opens/PROFILE 2 RESTRICTED bore Report 34 4/26/217 Time Summary Start Hours PH OPN Detail Drilled Depth level Rig Rate Description : 1.5 MNH1 RDP 18,737. REMOVE WEAR BUSHING. SET BPV. BLOW OUT CHOKE LINES & KILL LINES. 1:3 4.5 MNH1 WHD 18,737. N/D BOP LINES. NIPPLE DOWN BOPS. REMOVE CHOKE LINE, KILL LINE VALVES. L/D BOP HANDLER. INSTALL DUST CAP. RELEASE F/ 6 Total 6. MD Inc. Azi. TVD N/S Deepest 5 Surveys E/W V.Sec DLeg ( /1ft) 17, , , , PTW MWD_216 17, , , , PTW MWD_216 17, , , , PTW MWD_216 17, , , , PTW MWD_216 18, , , , PTW MWD_216 Fluid Details Mud type Invermul Oil/Water (%) POM (cc) MD TS/HGS/LGS (%) CaCl2 (%) Mud Density (ppg) Sand (%) Caom/Clom (ppm) Vis (s/qt) Oil/Water Ratio (%) ACT PV/YP (cp/lbf/1ft²) XS Lime(lbm/bbl) Gels 1 s/m (lbf/1ft²) LCM (lbm/bbl) ES (Volts) API/HTHP WL (cc/3min) ECD (ppg) R6/3 FC/HTHP FC (32nd") H2S (gas unit) R2/1 WPS (ppm) KCl (%) R6/3 FL temp. ( F) FUEL ON LOCATION: GAL FUEL RETURNED: 7 GAL Ditch Magnet in Last 24hrs/Cum. (gm) Remarks Tool

18 Report 1 11/21/216 Company Type bore WBS No/API No PERMIAN Development / Event Summary Event Type Drilling only Event Start Date 11/21/216 Days on Location.27 Objective Drill - Wolfcamp HZ Original Spud Date 11/21/216 Days Since Spud.4 Est. Days 2. Contractor PRECISION Work Unit PRECISION 565 Days To Release Rig Phone/FAX No. Status Supervisor Bryan Boyles Measured Depth 222. Engineer Robert Hahn TVD Other Supervisor Austin Mallet 24 Hr Progress 82. Depth Ref/Grd Elev/Water Depth DFE: 2,882.3 / 2,856.3 Hole size THF Datum Daily (hr/%) / Days Ahd(-) Bhnd(+)(5/5) Last Casing MD Next Casing MD Current Fluid Density(ppg) LOT/FIT EMW(ppg) Lithology Formation/MD Top 2.in@146.ft 9.625in@5,.ft Last Incident HSE Summary Date Days Last Incident Date Days KPI's LWC RWC MTC FAC Last casing pressure test PSI NII HPI GOAL ZERO DAYS PS BARRIER EVENT PS barrier bowtie review 1/24/ TRCF LWCF Safety Cards - Safe Safety Card - Unsafe SSE% Last casing pressure(psi) Safety Comments: 24 Hour Summary Walked rig, Post walk R/U, P/U BHA #1 and drilled T/ 222' Update Since Report Time Drilling ahead at 94' 24 Hour Forecast Continue drilling surface section Operations Summary 12/5/216 1:51:47 Report Version: R4 Generated from data in EDM/Opens/PROFILE 1

19 bore Report 1 11/21/216 Time Summary Start Hours PH OPN Detail Drilled Depth level Description 17:3.5 M RIT 146. HOLD PJSM ON WALKING 18:.5 M RIT 146. WALK, CENTER AND LEVEL OVER WELL 18:3 1. M RIT 146. WALK CATWALK AND LEVEL AND STRAIGHTEN, ADJUST SUITCASES 19:3 2:.5 M RGU M RGU 146. SPOT MATTING, GROUND, HOOK UP EASY RIDERS AND ESCAPE LINE SET TROUGH, R/U PVC IN BACKYARD, N/U CONDUCTOR RISER 22: 2 1. SRF1 BHA 146. HOLD PJSM AND P/U BHA #1 23: 1. SRF1 DRL 222. ROTATE DRILL F/ 14' T/ 222' 82 FPH) WOB: 2K RPM: SURF 4 MOTOR 9 BIT 13 PRESSURE: 1 PSI FLOW: 41 GPM TORQUE: ON BTM 12K P/U: 7K S/O: 5K ROT: 6K MW: 8.9 MOTOR REV/GAL:.22 Total Update Start Hours PH OPN Detail Drilled Depth level Description :.5 SRF1 DRL 315. ROTATE DRILL F/ 222' T/ 315' 186 FPH) WOB: 2K RPM: SURF 8 MOTOR 88 BIT 168 PRESSURE: 12 PSI FLOW: 4 GPM TORQUE: ON BTM 6K P/U: 8K S/O: 7K ROT: 75K MW: 8.9 MOTOR REV/GAL:.22 :3.5 SRF1 DRL 358. SLIDE DRILL F/ 315' T/ 358' 86 FPH) WOB: 2K RPM: SURF MOTOR 88 BIT 88 PRESSURE: 16 PSI FLOW: 4 GPM TORQUE: ON BTM K P/U: 9K S/O: 8K ROT: 85K MW: 8.9 MOTOR REV/GAL:.22 1:.5 SRF1 DRL 411. ROTATE DRILL F/ 358' T/ 411' 16 FPH) WOB: 2K RPM: SURF 8 MOTOR BIT PRESSURE: 18 PSI FLOW: 67 GPM TORQUE: ON BTM 1K P/U: 1K S/O: 9K ROT: 95K MW: 8.9 MOTOR REV/GAL:.22 1:3.5 SRF1 DRL 45. SLIDE DRILL F/ 411' T/ 45' 78 FPH) WOB: 3K RPM: SURF MOTOR 176 BIT 176 PRESSURE: 25 PSI FLOW: 8 GPM TORQUE: ON BTM K P/U: 11K S/O: 1K ROT: 15K MW: 8.9 MOTOR REV/GAL:.22 2: 1.5 SRF1 DRL 78. ROTATE DRILL F/ 45' T/ 78' 22 FPH) WOB: 3K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 3 PSI FLOW: 85 GPM TORQUE: ON BTM 12K P/U: 12K S/O: 11K ROT: 115K 12/5/216 1:51:47 Report Version: R4 Generated from data in EDM/Opens/PROFILE 2

20 bore Report 1 11/21/ Update Start Hours PH OPN Detail Drilled Depth level Description MW: 8.9 MOTOR REV/GAL:.22 3:3.5 SRF1 DRL 827. SLIDE DRILL F/ 78' T/ 827' 94 FPH) WOB: 3K RPM: SURF MOTOR 187 BIT 187 PRESSURE: 32 PSI FLOW: 85 GPM TORQUE: ON BTM K P/U: 14K S/O: 11K ROT: 125K MW: 8.9 MOTOR REV/GAL:.22 4: 1.5 SRF1 DRL 1,158. ROTATE DRILL F/ 827' T/ 1158' 22.7 FPH) WOB: 3K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 32 PSI FLOW: 85 GPM TORQUE: ON BTM 12K P/U: 14K S/O: 11K ROT: 125K MW: 8.9 MOTOR REV/GAL:.22 5:3.5 SRF1 SVC 1,158. Rig Service MD Inc. Azi. TVD N/S Deepest 5 Surveys E/W V.Sec DLeg ( /1ft) EPW MWD EPW MWD Bit Details Bit no. Size Manufacturer Model no. Class IADC Serial Size MD in MD out IADC Dull Grade code no. (32nd") HALLIBURTON SF65D x , CT-N-X-I-WT-TD Tool MD 222. WOB Min/Max Current RPM (rpm) Flow rate (gpm) SPP (psi) P bit (psi) Bit Operations Bit HHP (hp) Hours (hr) Footage ROP (ft/hr) Hours cum (hr) Footage cum. 2./ , ROP cum. (ft/hr) Item description 4" DRILL PIPE 18 JTS 5" HWDP CROSSOVER 6.5" DRILL COLLARS CROSSOVER FLOAT SUB FILTER SUB CROSSOVER 12" STEEL STABILIZER 8" NON-MAG DRILL COLLAR 12" NON-MAG STABILIZER NON-MAG DRILL COLLAR W/MWD # Jts Length Drillstring Components OD Max OD ID Connection Name Weight (ppf) Grade Serial no , XT XT /2 IF DR /2 XH /2 XH DR /2 IF DR /2 IF DR /2 IF DR /8 REG DR /8 REG DR /8 REG DR /8 REG D8L288K 12/5/216 1:51:47 Report Version: R4 Generated from data in EDM/Opens/PROFILE 3

21 bore Report 1 11/21/216 Item description NON-MAG CROSSOVER 12" STABILIZER # Jts Length Drillstring Components OD Max OD ID Connection Name Weight (ppf) Grade Serial no /2 IF DR /8 REG DR1818 8" BAKER MUD MOTOR 7/8 LOBE, STAGE BIT #1 RUN # " HALLIBURTON SF65D /8 REG /8 REG Drillstring Details Date/Time in Date/Time out BHA no. BHA Length Min. ID Purpose 11/21/216 23: 11/23/216 2: 1 1, DRILL 12.25" SURFACE SECTION MD 222. SW Up 7. SW Down 5. SW Rotn 6. Drag 1. Tq On Btm (ft-lbf) 12,. Tq Off Btm (ft-lbf) Footage 82. PUMP/HYDRAULIC DATA Pump Type Make/Model Stroke No. 1 JIAOZUO JINBIAO / JF Liner size Efficiency (%) Pressure (psi) SPM (spm) Output (gpm) Kill SPM/Pressure/Depth (spm/psi/ft) 2 JIAOZUO JINBIAO / JF /5/216 1:51:47 Report Version: R4 Generated from data in EDM/Opens/PROFILE 4

22 Report 2 11/22/216 Company Type bore WBS No/API No PERMIAN Development / Event Summary Event Type Drilling only Event Start Date 11/21/216 Days on Location 1.27 Objective Drill - Wolfcamp HZ Original Spud Date 11/21/216 Days Since Spud 1.4 Est. Days 2. Contractor PRECISION Work Unit PRECISION 565 Days To Release Rig Phone/FAX No. Status Supervisor Bryan Boyles Measured Depth 3,849. Engineer Robert Hahn TVD 3,792.4 Other Supervisor Austin Mallet 24 Hr Progress 3,627. Depth Ref/Grd Elev/Water Depth DFE: 2,882.3 / 2,856.3 Hole size THF Datum Daily (hr/%) / Days Ahd(-) Bhnd(+)(5/5) Last Casing MD 2.in@146.ft Next Casing MD 9.625in@5,.ft Current Fluid Density(ppg) 1. LOT/FIT EMW(ppg) Lithology Formation/MD Top Last Incident HSE Summary Date Days Last Incident Date Days KPI's LWC RWC MTC FAC Last casing pressure test PSI NII HPI GOAL ZERO DAYS PS BARRIER EVENT PS barrier bowtie review 1/24/ TRCF LWCF Safety Cards - Safe Safety Card - Unsafe SSE% Last casing pressure(psi) Safety Comments: GOAL ZERO DAYS: 466 DAYS SINCE LAST LTI: 466 DAYS SINCE LAST HIPO: 33 DAYS SINCE LAST MTC: 466 DAYS SINCE LAST LOPC: 466 Man Hours: hrs HSE Drills Drills/Tests Date Days Since Last Last Derrick Inspection Last BOP function test Last BOP Test Next BOP Test JSA's/Toolbox Talks Days Since Last Drill 1 24 Hour Summary Drilled surface F/ 222' T/ 3849' Update Since Report Time Drilling ahead at 41' 24 Hour Forecast Operations Summary Continue drilling surface to TD, POOH and L/D BHA, Run 9-5/8" casing, Perform 9-5/8" cement job 12/5/216 1:52:15 Report Version: R4 Generated from data in EDM/Opens/PROFILE 1

23 bore Report 2 11/22/216 Time Summary Start Hours PH OPN Detail Drilled Depth level Description :.5 SRF1 DRL 315. ROTATE DRILL F/ 222' T/ 315' 186 FPH) WOB: 2K RPM: SURF 8 MOTOR 88 BIT 168 PRESSURE: 12 PSI FLOW: 4 GPM TORQUE: ON BTM 6K P/U: 8K S/O: 7K ROT: 75K MW: 8.9 MOTOR REV/GAL:.22 :3.5 SRF1 DRL 358. SLIDE DRILL F/ 315' T/ 358' 86 FPH) WOB: 2K RPM: SURF MOTOR 88 BIT 88 PRESSURE: 16 PSI FLOW: 4 GPM TORQUE: ON BTM K P/U: 9K S/O: 8K ROT: 85K MW: 8.9 MOTOR REV/GAL:.22 1:.5 SRF1 DRL 411. ROTATE DRILL F/ 358' T/ 411' 16 FPH) WOB: 2K RPM: SURF 8 MOTOR BIT PRESSURE: 18 PSI FLOW: 67 GPM TORQUE: ON BTM 1K P/U: 1K S/O: 9K ROT: 95K MW: 8.9 MOTOR REV/GAL:.22 1:3.5 SRF1 DRL 45. SLIDE DRILL F/ 411' T/ 45' 78 FPH) WOB: 3K RPM: SURF MOTOR 176 BIT 176 PRESSURE: 25 PSI FLOW: 8 GPM TORQUE: ON BTM K P/U: 11K S/O: 1K ROT: 15K MW: 8.9 MOTOR REV/GAL:.22 2: 1.5 SRF1 DRL 78. ROTATE DRILL F/ 45' T/ 78' 22 FPH) WOB: 3K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 3 PSI FLOW: 85 GPM TORQUE: ON BTM 12K P/U: 12K S/O: 11K ROT: 115K MW: 8.9 MOTOR REV/GAL:.22 3:3.5 SRF1 DRL 827. SLIDE DRILL F/ 78' T/ 827' 94 FPH) WOB: 3K RPM: SURF MOTOR 187 BIT 187 PRESSURE: 32 PSI FLOW: 85 GPM TORQUE: ON BTM K P/U: 14K S/O: 11K ROT: 125K MW: 8.9 MOTOR REV/GAL:.22 4: 1.5 SRF1 DRL 1,158. ROTATE DRILL F/ 827' T/ 1158' 22.7 FPH) WOB: 3K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 32 PSI FLOW: 85 GPM TORQUE: ON BTM 12K P/U: 14K S/O: 11K ROT: 125K MW: 8.9 MOTOR REV/GAL:.22 5:3.5 SRF1 SVC 1,158. Rig Service 6: 2.5 SRF1 DRL 1,77. ROTATE DRILL F/ 1158' T/ 177' FPH) WOB: 35K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM 14K P/U: 175K S/O: 15K ROT: 165K MW: 8.9 MOTOR REV/GAL:.22 12/5/216 1:52:15 Report Version: R4 Generated from data in EDM/Opens/PROFILE 2

24 bore Report 2 11/22/216 Time Summary Start Hours PH OPN Detail Drilled Depth level Description 8:3.5 SRF1 DRL 1,733. SLIDE DRILL F/ 177' T/ 1733' 52 FPH) WOB: 35K RPM: SURF MOTOR 187 BIT 187 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM K P/U: 175K S/O: 15K ROT: 165K MW: 9.3 MOTOR REV/GAL:.22 9: 3. SRF1 DRL 2,424. ROTATE DRILL F/ 1733' T/ 2424' 23.3 FPH) WOB: 35K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM 14K P/U: 175K S/O: 15K ROT: 165K MW: 9.8 MOTOR REV/GAL:.22 12:.5 SRF1 DRL 2,459. SLIDE DRILL F/ 2424' T/ 2459' 7 FPH) WOB: 35K RPM: SURF MOTOR 187 BIT 187 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM K P/U: 175K S/O: 15K ROT: 165K MW: 9.8 MOTOR REV/GAL:.22 12:3 4. SRF1 DRL 3,221. ROTATE DRILL F/ 2459' T/ 3221' 19.5 FPH) WOB: 35K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM 14K P/U: 175K S/O: 15K ROT: 165K MW: 9.8 MOTOR REV/GAL:.22 16:3.5 SRF1 SVC 3,221. GREASE BLOCK AND TOP DRIVE 17: 18: 18:3 19:3 1. SRF1 DRL 3,32..5 SRF1 DRL 3, SRF1 DRL 3, SRF1 DRL 3,529. ROTATE DRILL F/ 3221' T/ 332' 99 FPH) WOB: 35K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM 14K P/U: 175K S/O: 15K ROT: 165K MW: 9.8 MOTOR REV/GAL:.22 ROTATE DRILL F/ 332' T/ 341' 162 FPH) WOB: 45K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 118 PSI FLOW: 85 GPM TORQUE: ON BTM 16K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 SLIDE DRILL F/ 341' T/ 3421' 2 FPH) WOB: 45K RPM: SURF MOTOR 187 BIT 187 PRESSURE: 118 PSI FLOW: 85 GPM TORQUE: ON BTM K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 ROTATE DRILL F/ 3421' T/ 3529' 18 FPH) WOB: 45K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 118 PSI FLOW: 85 GPM TORQUE: ON BTM 16K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 12/5/216 1:52:15 Report Version: R4 Generated from data in EDM/Opens/PROFILE 3

25 bore Report 2 11/22/216 Time Summary Start Hours PH OPN Detail Drilled Depth level Description 2:3 1. SRF1 DRL 3,58. SLIDE DRILL F/ 3529' T/ 358' 51 FPH) WOB: 45K RPM: SURF MOTOR 187 BIT 187 PRESSURE: 118 PSI FLOW: 85 GPM TORQUE: ON BTM K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 21:3 1. SRF1 DRL 3,711. ROTATE DRILL F/ 358' T/ 3711' 131 FPH) WOB: 45K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 118 PSI FLOW: 85 GPM TORQUE: ON BTM 16K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 22:3.5 SRF1 DRL 3,751. SLIDE DRILL F/ 3711' T/ 3751' 8 FPH) WOB: 45K RPM: SURF MOTOR 187 BIT 187 PRESSURE: 118 PSI FLOW: 85 GPM TORQUE: ON BTM K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 23: 1. SRF1 DRL 3,849. ROTATE DRILL F/ 3751' T/ 3849' 98 FPH) WOB: 45K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 118 PSI FLOW: 85 GPM TORQUE: ON BTM 16K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 Total Update Start Hours PH OPN Detail Drilled Depth level Description : 4.5 SRF1 DRL 4,248. ROTATE DRILL F/ 3849' T/ 4248' 88.7 FPH) WOB: 45K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM 16K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 4:3.5 SRF1 DRL 4,278. SLIDE DRILL F/ 4248' T/ 4278' 6 FPH) WOB: 45K RPM: SURF MOTOR 187 BIT 187 PRESSURE: 35 PSI FLOW: 85 GPM TORQUE: ON BTM K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 5:.5 SRF1 DRL 4,298. ROTATE DRILL F/ 4278' T/ 4298' 4 FPH) WOB: 45K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM 16K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 5:3.5 SRF1 SVC 4,298. SERVICE 12/5/216 1:52:15 Report Version: R4 Generated from data in EDM/Opens/PROFILE 4

26 bore Report 2 11/22/216 Deepest 5 Surveys MD Inc. Azi. TVD N/S E/W V.Sec DLeg ( /1ft) 3, , EPW MWD 3, , EPW MWD 3, , EPW MWD 3, , EPW MWD 3, , EPW MWD Fluid Details Mud type NaCl Brine Oil/Water (%)./88.8 ph/pm (cc) 9.5/.2 MD 3,216. TS/HGS/LGS (%) 1.4/.3/1.1 Pf/Mf (cc).1/.15 Mud Density (ppg) 1. Sand (%).1 Ca+ (ppm) Vis (s/qt) Cl- (ppm) 167, PV/YP (cp/lbf/1ft²) 1./3. MBT (lbm/bbl) Gels 1 s/m (lbf/1ft²) 1./1. LCM (lbm/bbl) API/HTHP WL (cc/3min) 1./ ECD (ppg) 1.4 R6/3 FC/HTHP FC (32nd") 3./ H2S (gas unit) R2/1 KCl (%) R6/3 FL temp. ( F) Ditch Magnet in Last 24hrs/Cum. (gm) Bit Details Bit no. Size Manufacturer Model no. Class IADC Serial Size MD in MD out IADC Dull Grade code no. (32nd") HALLIBURTON SF65D x , CT-N-X-I-WT-TD Tool MD ,158. 1,77. 1,733. 2,424. 2,459. 3,221. 3,32. 3,41. 3,421. 3,529. 3,58. 3,711. 3,751. 3,849. WOB Min/Max Current RPM (rpm) Flow rate (gpm) SPP (psi) P bit (psi) Bit Operations Bit HHP (hp) Hours (hr) Footage ROP (ft/hr) Hours cum (hr) Footage cum. 2./ , / , / , / , / , / , / , , / , , / , , / , , / , , / , , / , , / , , / , , / , , / , , / , , / , , / , , ROP cum. (ft/hr) Item description 4" DRILL PIPE 18 JTS 5" HWDP CROSSOVER # Jts Length Drillstring Components OD Max OD ID Connection Name Weight (ppf) Grade Serial no , XT XT /2 IF DR /5/216 1:52:15 Report Version: R4 Generated from data in EDM/Opens/PROFILE 5

27 bore Report 2 11/22/216 Item description 6.5" DRILL COLLARS CROSSOVER FLOAT SUB FILTER SUB CROSSOVER 12" STEEL STABILIZER 8" NON-MAG DRILL COLLAR 12" NON-MAG STABILIZER NON-MAG DRILL COLLAR W/MWD NON-MAG CROSSOVER 12" STABILIZER # Jts Length Drillstring Components OD Max OD ID Connection Name Weight (ppf) Grade Serial no /2 XH /2 XH DR /2 IF DR /2 IF DR /2 IF DR /8 REG DR /8 REG DR /8 REG DR /8 REG D8L288K /2 IF DR /8 REG DR1818 8" BAKER MUD MOTOR 7/8 LOBE, STAGE BIT #1 RUN # " HALLIBURTON SF65D /8 REG /8 REG Drillstring Details Date/Time in Date/Time out BHA no. BHA Length Min. ID Purpose 11/21/216 23: 11/23/216 2: 1 1, DRILL 12.25" SURFACE SECTION MD 315. SW Up 8. SW Down 7. SW Rotn 75. Drag 5. Tq On Btm (ft-lbf) 6,. Tq Off Btm (ft-lbf) Footage ,158. 1,77. 1,733. 2,424. 2,459. 3,221. 3,32. 3,41. 3,421. 3,529. 3,58. 3,711. 3,751. 3, , , , , , , , , , , ,. 98. PUMP/HYDRAULIC DATA Pump Type Make/Model Stroke No. 1 JIAOZUO JINBIAO / JF Liner size Efficiency (%) Pressure (psi) SPM (spm) Output (gpm) Kill SPM/Pressure/Depth (spm/psi/ft) 2 JIAOZUO JINBIAO / JF /5/216 1:52:15 Report Version: R4 Generated from data in EDM/Opens/PROFILE 6

28 bore Report 2 11/22/216 Fuel on Location: gal Fuel Used: 2743 gal Fuel Received: 74 gal Remarks 12/5/216 1:52:15 Report Version: R4 Generated from data in EDM/Opens/PROFILE 7

29 Report 3 11/23/216 Company Type bore WBS No/API No PERMIAN Development / Event Summary Event Type Drilling only Event Start Date 11/21/216 Days on Location 2.27 Objective Drill - Wolfcamp HZ Original Spud Date 11/21/216 Days Since Spud 2.4 Est. Days 2. Contractor PRECISION Work Unit PRECISION 565 Days To Release Rig Phone/FAX No. Status Supervisor Bryan Boyles Measured Depth 5,61. Engineer Robert Hahn TVD 4, Other Supervisor Austin Mallet 24 Hr Progress 1,212. Depth Ref/Grd Elev/Water Depth DFE: 2,882.3 / 2,856.3 Hole size THF Datum Daily (hr/%) / Days Ahd(-) Bhnd(+)(5/5) Last Casing MD 2.in@146.ft Next Casing MD 9.625in@5,.ft Current Fluid Density(ppg) 1.5 LOT/FIT EMW(ppg) Lithology Formation/MD Top Last Incident HSE Summary Date Days Last Incident Date Days KPI's LWC RWC MTC FAC Last casing pressure test PSI NII HPI GOAL ZERO DAYS PS BARRIER EVENT PS barrier bowtie review 1/24/ TRCF LWCF Safety Cards - Safe Safety Card - Unsafe SSE% Last casing pressure(psi) Safety Comments: GOAL ZERO DAYS: 467 DAYS SINCE LAST LTI: 467 DAYS SINCE LAST HIPO: 34 DAYS SINCE LAST MTC: 467 DAYS SINCE LAST LOPC: 467 Man Hours: 165 hrs HSE Drills Drills/Tests Date Days Since Last Last Derrick Inspection Last BOP function test Last BOP Test Next BOP Test JSA's/Toolbox Talks Days Since Last Drill 2 24 Hour Summary Operations Summary Drill surface F/ 3849' T/ 561', Performed clean up cycles and POOH, L/D BHA, R/U Tesco and run 9-5/8" casing T/ 168' Update Since Report Time Running 9-5/8" casing at 485' 24 Hour Forecast Run 9-5/8" casing T/ 561', Circulate casing volume, R/D Tesco and R/U Baker cementers, Perform surface cement job 12/5/216 1:52:23 Report Version: R4 Generated from data in EDM/Opens/PROFILE 1

30 bore Report 3 11/23/216 Time Summary Start Hours PH OPN Detail Drilled Depth level Description : 4.5 SRF1 DRL 4,248. ROTATE DRILL F/ 3849' T/ 4248' 88.7 FPH) WOB: 45K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM 16K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 4:3.5 SRF1 DRL 4,278. SLIDE DRILL F/ 4248' T/ 4278' 6 FPH) WOB: 45K RPM: SURF MOTOR 187 BIT 187 PRESSURE: 35 PSI FLOW: 85 GPM TORQUE: ON BTM K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 5:.5 SRF1 DRL 4,298. ROTATE DRILL F/ 4278' T/ 4298' 4 FPH) WOB: 45K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 36 PSI FLOW: 85 GPM TORQUE: ON BTM 16K P/U: 2K S/O: 16K ROT: 18K MW: 1 MOTOR REV/GAL:.22 5:3.5 SRF1 SVC 4,298. SERVICE 6: 13: 7. SRF1 DRL 5, SRF1 CBU 5,61. ROTATE DRILL F/ 4298' T/ 561' 19 FPH) WOB: 45K RPM: SURF 8 MOTOR 187 BIT 267 PRESSURE: 425 PSI FLOW: 85 GPM TORQUE: ON BTM 15K P/U: 22K S/O: 18K ROT: 2K MW: 1 MOTOR REV/GAL:.22 PUMP SWEEPS AND SLUG 14: 1.5 SRF1 TOH 5,61. POOH F/ 561' T/ 1165', PULL ROT HEAD 15:3 16:3 2: 1. SRF1 TOH 5,61. POOH F/ 1165' T/ 9' 3.5 SRF1 BHA 5,61. L/D BHA #1 BIT #1 GRADE: 2-1-CT-N-X-I-WT-TD 4. SRF1 CLR 5,61. RU TESCO AND RUN 9-5/8" CASING T/ 168' Total Update Start Hours PH OPN Detail Drilled Depth level Description : 2. SRF1 CLR 5,61. RUN 9 5/8" CSG F/ 1723' T/ 3456'. HELD SAFETY STAND DOWN W/ CREW AND CSG CREW ON STAYING FOCUSED ON JOB 2: 2.5 SRF1 CLR 5,61. RUN 9 5/8" CSG F/ 3456' T/ 561' 4:3.5 SRF1 RCC 5,61. INSTALL CSG SWEDGE & DOWN TESCO. HELD STAND DOWN W/ CREW AND CSG CREW ON DOWN 5: 1. SRF1 RCC 5,61. CIRCULATE WHILE WAITING ON CEMENT TO ARRIVE ON LOCATION MD Inc. Azi. TVD N/S Deepest 5 Surveys E/W V.Sec DLeg ( /1ft) 4, , EPW MWD 12/5/216 1:52:23 Report Version: R4 Generated from data in EDM/Opens/PROFILE 2 Tool

EP WELLS DAILY OPERATIONS REPORT Report 1 02/02/2017

EP WELLS DAILY OPERATIONS REPORT Report 1 02/02/2017 Report 2/2/27 Company Type WBS No/API No PERMIAN Development 3259585 / 423337 Event Summary Event Type Drilling only Event Start Date 2/2/27 Days on Location.94 Objective Drill - Wolfcamp Shale Original

More information

EP WELLS DAILY OPERATIONS REPORT Report 19 05/26/2016

EP WELLS DAILY OPERATIONS REPORT Report 19 05/26/2016 Report 19 5/26/216 Company Type WBS No/API No PERMIAN Exploration 324861 / 423132849. Event Summary Event Type Drilling only Event Start Date 4/24/216 Days on Location 18.67 Objective Drill - Wolfcamp

More information

EP WELLS DAILY OPERATIONS REPORT Report 29 05/19/2017

EP WELLS DAILY OPERATIONS REPORT Report 29 05/19/2017 5/2/27 5:23:5 Report Version: 4..6R9 Generated from data in EDM/Opens/PROFILE Report 29 5/9/27 Company Type WBS No/API No PERMIAN Development UNIVERSITY 9 PW UNIT 56H UNIVERSITY 9 PW UNIT 56H 32656 / 4233326.

More information

EP WELLS DAILY OPERATIONS REPORT Report 38 07/18/2017

EP WELLS DAILY OPERATIONS REPORT Report 38 07/18/2017 1 Company Type bore WBS No/API No PERMIAN Development 30265014 / 4230133171.00 Event Summary Event Type Completion only Event Start Date 04/28/2017 Days on Location 37.00 Objective Install Completion Original

More information

Drilling Morning Report

Drilling Morning Report REPORT DATE 5/0/200 Report # AFE # Casing OD(in) WT(lbs/ft) Grade Btm MD(ft) Btm TVD(ft) DCRB04 TVD: 32 MD: 32 Progress: 32 Planned TD:,500 Current Hole Size: Days From Spud: Spud Date: 5//0 Days on Well:

More information

Terrace Petroleum Corporation Cunning Wolf UL No. 602H, 1980 FNL and 467 FWL Section 6, Block 23, ULS Pecos County, Texas

Terrace Petroleum Corporation Cunning Wolf UL No. 602H, 1980 FNL and 467 FWL Section 6, Block 23, ULS Pecos County, Texas Terrace Petroleum Corporation Cunning Wolf UL No. 602H, 1980 FNL and 467 FWL Section 6, Block 23, ULS Pecos County, Texas 3-29-13 DAY 1 Previously built location, roads, built and lined reserve pits. Move

More information

EP WELLS DAILY OPERATIONS REPORT Report 1 08/03/2016

EP WELLS DAILY OPERATIONS REPORT Report 1 08/03/2016 Report 1 8/3/216 Company Type bore WBS No/API No PERMIAN Exploration / 424953375. Event Summary Event Type Completion only Event Start Date 8/3/216 Days on Location 1. Objective Install Completion Original

More information

University 31E 4. Ward County, TX. Rig: Union Drlg Rig 229. AFE: $1,393, DHC: $761, WI: Notes: Workover:

University 31E 4. Ward County, TX. Rig: Union Drlg Rig 229. AFE: $1,393, DHC: $761, WI: Notes: Workover: Zone: War-Wink Cherry Canyon TD: 7250' Rig: Union Drlg Rig 229 Status: WOC Spud Date: 1/26/2013 RR Date: 2/12/2013 First Sales: AFE: $1,393,293.00 DHC: $761,963.00 WI: Notes: Date Activity 11/14/2012 11/14/12

More information

AMERICAN ENERGY - PERMIAN BASIN, LLC UL Daily Drilling Partner Summary

AMERICAN ENERGY - PERMIAN BASIN, LLC UL Daily Drilling Partner Summary AEPB WELL NO. Report End Date: Report Number: 1 Rig: INTEGRITY, 3 Projected Days (days): 0 Drilling Days: : 70 : 0 Planned VS (ft): Current VS (ft): 42383383570000 MIRU MIRU INTEGRITY 3. 70 Longitude Orig

More information

D & V Oil Co. LP. Daily Completion Report - University CN A #6 API # /23/2016. Perfs ' ' Activity :

D & V Oil Co. LP. Daily Completion Report - University CN A #6 API # /23/2016. Perfs ' ' Activity : Daily Completion Report - University CN A #6 API # 42-105-42334 12/23/2016 Activity at Report Time: Perfs - 2512' - 2632' Depth at Report Time Put Well on Production 2655' - PBTD Activity : Arrive Location.

More information

PERMIAN RESOURCES, LLC UL Daily Drilling Partner Summary

PERMIAN RESOURCES, LLC UL Daily Drilling Partner Summary PRES WELL NO. Report End Date: 5/19/2016 Report Number: 3 Rig: INTEGRITY, 3 Projected Days (days): 0 Drilling Days: : : 0 Planned VS (ft): Current VS (ft): WOC WOC, CONTACTED TRRC, SPOKE TO ABRAHAM, ADVISED

More information

Niko Deepwater Weatherford MPD DODI Ocean Monarch Nelson Emery Niko Indonesia Drilling Superintendent

Niko Deepwater Weatherford MPD DODI Ocean Monarch Nelson Emery Niko Indonesia Drilling Superintendent Niko Deepwater Weatherford MPD DODI Ocean Monarch Nelson Emery Niko Indonesia Drilling Superintendent 26 Feb - 2014 SPE Thailand 1 Outline Drivers for MPD: 1. Safety of personnel in remote operations 2.

More information

Wellwork Chronological Regulatory Report

Wellwork Chronological Regulatory Report Well Name: UNIVERSITY 49 #0808H Field: Lin (Wolfcamp) S/T/R: / / County, State: Location Desc: Operator: Enduring Resources, LLC Project Type: Completion District: Southern Project AFE: DV02151 AFE's Associated:

More information

SUBSEA KILL SHEET EXERCISE No. 5

SUBSEA KILL SHEET EXERCISE No. 5 Subsea Kill Sheet Exercise No. 5 SUBSEA KILL SHEET EXERCISE No. 5 Name: Date: Complete the Subsea vertical kill sheet provided on pages 2 and 3. Then answer questions 1 to 12. Please round calculations

More information

BP SIT Testing Franks Facility Lafayette

BP SIT Testing Franks Facility Lafayette BP SIT Testing Franks Facility Lafayette General Information Status: Franks test well Lafayette La. Rig: Franks Test Rig Casing: 13 3/8, 0 to 4,600 Workstring: 4 ½ IF Brine: Fresh Water Directional: Straight

More information

ENDEAVOR ENERGY RESOURCES

ENDEAVOR ENERGY RESOURCES ENDEAVOR ENERGY RESOURCES Lease WELL NO FIELD PBTD PERFORATIONS FOREMAN TOOLPUSHER API NUMBER DATE University 5-20-21 #1H 14,223' Tony Cody 07/02/13 OART WEATHER FLUID SUMMARY W/O UNIT DATA W/L UNIT DATA

More information

and and Norton J. Lapeyrouse CONTENTS

and and Norton J. Lapeyrouse CONTENTS and and Norton J. Lapeyrouse CONTENTS Chapter 1 Basic Formulas P. 3 1. 2. 3. 4. 5. 6. 7. 8. 9. 10. 11. 12. 13. 14. 15. 16. 17. 18. 19. Pressure Gradient Hydrostatic Pressure Converting Pressure into Mud

More information

W I L D W E L L C O N T R O L CIRCULATION & WELL CONTROL

W I L D W E L L C O N T R O L CIRCULATION & WELL CONTROL CIRCULATION & WELL CONTROL Learning Objectives You will learn: The importance of pump rates and pressures during well control operations Pressure relationships Basic calculations necessary in well control

More information

FORGE Energy UL 21 Pahaska 1H API Number:

FORGE Energy UL 21 Pahaska 1H API Number: FORGE Energy UL 21 Pahaska 1H API Number: 42-495-33740 10/26/2016 07:00 HPJM 07:15 Install 1502 Adapter Flanges to Well Head. RU Pump Truck test lines to 1000 PSI no leaks. Load hole w/ 15 bbls fresh water.

More information

Study Guide IADC WellSharp Driller and Supervisor

Study Guide IADC WellSharp Driller and Supervisor Times to Flow Check: Before pulling out of the hole Before pulling BHA into the BOP When bit is pulled into the casing Increase in cuttings at shakers with same ROP On connections Upon abnormal trip tank

More information

BENEDUM (DEVONIAN, GAS) API # UPTON COUNTY, TX DRILLING PERMIT # DAILY REPORTS

BENEDUM (DEVONIAN, GAS) API # UPTON COUNTY, TX DRILLING PERMIT # DAILY REPORTS 11/17/2011 11/18/2011 11/19/2011 AFE dated 11/18/2011 - pull tbg out of hole and make a mill run. Run packer on tbg and attempt to reestablish production from Devonian Formation. MIRU Great Basin Pulling

More information

Daily Drilling Report

Daily Drilling Report Daily Drilling Report Well Name UTL 38-17-1H Report Date 05/05/2014 Field University Lands Supervisor Nate Baxter Report No. 97 Location 990' FNL & 300' FEL Supervisor 2 Kevin Evans DFS 94 County Ward

More information

Final Well Report. Revision: Version 0. Corp) Hole Name: Flat Bay Test Hole # 5 Rig: Duralite 800

Final Well Report. Revision: Version 0. Corp) Hole Name: Flat Bay Test Hole # 5 Rig: Duralite 800 Final Well Report Revision: Version 0 Operating Company: Vulcan Minerals Inc. (Investcan Energy Corp) Hole Name: Flat Bay Test Hole # 5 Rig: Duralite 800 Field: Flat Bay Location: Western Newfoundland,

More information

HydroPull. Extended-Reach Tool. Applications

HydroPull. Extended-Reach Tool. Applications Extended-Reach Tool HydroPull This tool incorporates a cycling valve that momentarily interrupts the flow to create water-hammer pressure pulses inside coiled or jointed tubing used in horizontal well

More information

Rig Math. Page 1.

Rig Math. Page 1. Page 1 The Calculator and Main Keyboard Display Numerical 10-key pad used for entering numerical values Trigonometric Functions These keys will be used where wellbore angle is an issue These are the keys

More information

RIH intermediate section casing in Bazian-1 exploration oil well

RIH intermediate section casing in Bazian-1 exploration oil well Energy and Sustainability V 559 RIH intermediate section casing in Bazian-1 exploration oil well A. K. Darwesh Petroleum Engineering Department, Engineering Faculty, Koya University, Kurdistan Abstract

More information

DUO-SQUEEZE H LCM Mixing Tables and Operating Procedures

DUO-SQUEEZE H LCM Mixing Tables and Operating Procedures BAROID DUO-SQUEEZE H LCM Mixing Tables and Operating Procedures Prepared for: Prepared by: Submitted by: Submittal Date: All Customers Sharath Savari, Donald L. Whitfill Halliburton January 2014 1 Copyright

More information

FORGE Energy UL 21 Freedom 1 API Number:

FORGE Energy UL 21 Freedom 1 API Number: FORGE Energy UL 21 Freedom 1 API Number: 42-371-39061 07/13/2013 RU E&P WL Open well RIH correlate GR log to get on depth. Run BL found cement to surface. Tag 7566' PBTD. RU Rising Star test lines to 5000

More information

Horizontal Marmaton Wells in Beaver County, OK

Horizontal Marmaton Wells in Beaver County, OK Horizontal Marmaton Wells in Beaver County, OK Drilling Improvements & Lessons Learned Presented by: Michael Dunn Drilling Engineer Unit Petroleum Forward Looking Statement DISCLAIMER It is understood

More information

Practice Exam IADC WellSharp Driller and Supervisor

Practice Exam IADC WellSharp Driller and Supervisor Workover & Completion Day 4 1. In a workover operation of a shut in well a Lubricator is being used together with a Wireline BOP / Wireline Valve. Which Barrier is classified as the Primary Barrier? A.

More information

PROPOSED NEW SUB- CODE 1 RIG UP AND TEAR. Possibly Fits into Existing Code. 7/26/2018 Review PROPOSED NEW CODE EXISTING OPERATION

PROPOSED NEW SUB- CODE 1 RIG UP AND TEAR. Possibly Fits into Existing Code. 7/26/2018 Review PROPOSED NEW CODE EXISTING OPERATION NW NW 1 RIG UP AND TAR 1 no sub-code RIG UP AND TAR DOWN Start: Rig released from previous well, nd: Rig fully rigged up, acceptance tests successfully completed, and signed off. DOWN 1 1 Rig Under Tow

More information

DAY ONE. 2. Referring to the last question, what mud weight would be required to BALANCE normal formation pressure?

DAY ONE. 2. Referring to the last question, what mud weight would be required to BALANCE normal formation pressure? DAY ONE 1. Normal formation pressure gradient is generally assumed to be: A..496 psi/ft B..564 psi/ft C..376 psi/ft D..465 psi/ft 2. Referring to the last question, what mud weight would be required to

More information

Chapter 5 HORIZONTAL DRILLING

Chapter 5 HORIZONTAL DRILLING Chapter 5 HORIZONTAL DRILLING Chapter 5 How much money am I about to put on the table for a horizontal well? Did I do sufficient planning? Keys to Successful Horizontal Wells Multi-disciplined teams working

More information

Deepwater Horizon Incident Internal Investigation

Deepwater Horizon Incident Internal Investigation Not all Information has been verified or corroborated. Subject to review based on additional information or analysis. Deepwater Horizon Incident Internal Investigation 1 Areas of Discussion Investigation

More information

Post Job Summary Cement Intermediate Casing

Post Job Summary Cement Intermediate Casing EXXONMOBIL CORPORATION HOUSTON, Texas PCU 197-36A6 H&P 326 Post Job Summary Cement Intermediate Casing Prepared for: George McNary Date Prepared: November 16, 2010 Version: 1 Service Supervisor: ANDERSON,

More information

1. The well has been shut in on a kick and the kill operation has not started.

1. The well has been shut in on a kick and the kill operation has not started. Well Control Methods Day 2 1. The well has been shut in on a kick and the kill operation has not started. Shut in drill pipe pressure Shut in casing pressure 500 psi 700 psi After stabilization, both pressures

More information

Wellwork Chronological Regulatory Report

Wellwork Chronological Regulatory Report Well Name: UNIVERSITY 09A #1003H Field: Lin (Wolfcamp) S/T/R: / / County, State: Location Desc: Operator: Enduring Resources, LLC Project Type: Completion District: Southern - ERPBU Project AFE: DV02251

More information

6-3/4 DUAL PORTED PBL BYPASS SYSTEM (Applicable to sizes 6-1/4 & 6-1/2 also)

6-3/4 DUAL PORTED PBL BYPASS SYSTEM (Applicable to sizes 6-1/4 & 6-1/2 also) RECEIVING PBL AT RIG SITE TITLE: Operating Instructions for -3/4 PBL -3/4 DUAL PORTED PBL BYPASS SYSTEM (Applicable to sizes -1/4 & -1/2 also) OPERATING INSTRUCTIONS 1. On receipt of PBL Bypass Tools at

More information

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG RAILROAD COMMISSION OF TEXAS 1701 N. Congress P.O. Box 12967 Austin, Texas 78701-2967 Status: Form W-2 OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG Date: Tracking No.: Approved 10/13/2015

More information

Casing Design. Casing Design. By Dr. Khaled El-shreef

Casing Design. Casing Design. By Dr. Khaled El-shreef Casing Design By Dr. Khaled El-shreef 1 Casing Design CONTENTS Function of Casing Casing Types & Tools Strength Properties Casing Specification Casing Design 2 1 RUNNING AND CEMENTING CASING Reasons for

More information

2-7/8 TRIPLE PORTED PBL BYPASS SYSTEM

2-7/8 TRIPLE PORTED PBL BYPASS SYSTEM RECEIVING PBL AT RIG SITE TITLE: Operating Instructions for 2-7/8 Triple Port PBL 1-10-201 2-7/8 TRIPLE PORTED PBL BYPASS SYSTEM OPERATING INSTRUCTIONS 1. On receipt of PBL Bypass Tools at Rig site, the

More information

PHE KE30-A8 WORKOVER PROGRAM

PHE KE30-A8 WORKOVER PROGRAM PHE WMO KE30-A8 WORKOVER PROGRAM PHE KE30-A8 WORKOVER PROGRAM Prepared by: Ross Webber. Hendra Wahyudi. Chandra Maulana. George Lattimore Adi Benanjaya Achmad Soendaroe. Tri Wiyono DRILLING ENGINEER SR.

More information

MOCS. Multiple Opening Circulation Sub. Fluid Bypass Valve

MOCS. Multiple Opening Circulation Sub. Fluid Bypass Valve MOCS Multiple Opening Circulation Sub Fluid Bypass Valve 1 Applications BHA Protection o o Pumping LCM Spotting Acid Work-over and completions o o o Well bore cleanout Fluid displacements Bottoms-up circulation

More information

Greystone Oil & Gas Rig Telephone 832-380-6698 Daily Summary Information Daily Cost Information Rig Information Well Name & No Report # Date MD TVD AFE AFE Amount Company Rep University AZ #1 7 4/26/2010

More information

SCORPION HIGH-QUALITY, FULLY COMPOSITE PLUGS

SCORPION HIGH-QUALITY, FULLY COMPOSITE PLUGS SCORPION HIGH-QUALITY, FULLY COMPOSITE PLUGS A DIFFERENT KIND OF ENERGY COMPANY Nine Energy Service isn t your typical oilfield services company. Our success stems from a culture driven by performance

More information

DRILLSCENE PROACTIVE DRILLING DECISIONS

DRILLSCENE PROACTIVE DRILLING DECISIONS DRILLSCENE PROACTIVE DRILLING DECISIONS RISE TO THE CHALLENGE OF REAL-TIME DRILLING CONTROL Today s oil and gas drilling operations present significant technical challenges in remote locations and increasingly

More information

"Sharing To Be Better. Influx through failed cement in shoetrack during completion operations

Sharing To Be Better. Influx through failed cement in shoetrack during completion operations "Sharing To Be Better Influx through failed cement in shoetrack during completion operations 2 Well status completion operations Seabed @ 364m 7" liner cemented across reservoir Well filled with 1.54 SG

More information

IMPLEMENTATION DSIW-System ELDFISK ALPHA MARS 2011

IMPLEMENTATION DSIW-System ELDFISK ALPHA MARS 2011 IMPLEMENTATION DSIW-System ELDFISK ALPHA MARS 2011 Report: Wiping performance Pressure drop-rupture disc function-gas kick circulation Ketil Botnmark, Kjell Mikalsen 20.05.2011 This report resumes the

More information

float equipment OPERATING MANUAL TYPE 505/506 Float Equipment 1. INFORMATION & RECOMMENDATIONS Float Equipment

float equipment OPERATING MANUAL TYPE 505/506 Float Equipment 1. INFORMATION & RECOMMENDATIONS Float Equipment Contents 1. GENERAL INFORMATION & RECOMMENDATIONS 1 2. INSTALLATION FLOAT EQUIPMENT 2 2.1 PRE-USE FIELD INSPECTION 2 2.2 POSITION FLOAT ON CASING STRING 3 3. RUNNING OF FLOAT EQUIPMENT 3 3.1 CIRCULATION

More information

Hydro-Mech Bridge Plug

Hydro-Mech Bridge Plug Manual No: 0620000303 Revision: F Approved By: Quality Engineer Date: 2014-9-9 Hydro-Mech Bridge Plug DESCRIPTION: Map Hydro-Mech Bridge Plug is hydraulically actuated and mechanically set. Compact, with

More information

OCEAN DRILLING PROGRAM

OCEAN DRILLING PROGRAM BIH OCEAN DRILLING PROGRAM www.oceandrilling.org Scientifi c Application Packers A packer is an inflatable rubber element that inflates to seal the annular space between the drill string and the borehole

More information

PowerDrive X6. Rotary Steerable System for high-performance drilling and accurate wellbore placement

PowerDrive X6. Rotary Steerable System for high-performance drilling and accurate wellbore placement Rotary Steerable System for high-performance drilling and accurate wellbore placement The PowerDrive X6 RSS maintains control under the most difficult conditions, bringing the benefits of rotary steerable

More information

BANDAR PANJI-1 WELL CONTROL INCIDENT REPORT

BANDAR PANJI-1 WELL CONTROL INCIDENT REPORT BANDAR PANJI-1 WELL CONTROL INCIDENT REPORT EXECUTIVE SUMMARY I was requested by management to review the Banjar Panji-1 drilling operations from the conception of the Integrated Drilling Management approach

More information

BaraBlend -665 LCM Standard Field Application Procedure

BaraBlend -665 LCM Standard Field Application Procedure BAROID BaraBlend -665 LCM Standard Field Application Procedure Prepared for: Prepared by: Submitted by: Submittal Date: All Customers Sharath Savari, Donald L. Whitfill Halliburton Apr 2016 1 Copyright

More information

Bridge Plugs, Ball Drop & Caged Ball Plugs For Zone Isolation

Bridge Plugs, Ball Drop & Caged Ball Plugs For Zone Isolation Bridge Plugs, Ball Drop & Caged Ball Plugs For Zone Isolation ADVANTAGE composite bridge plug, caged ball and ball drop (flow thru) frac plug provide a means to isolate multiple zones during high pressure

More information

Optimising Hydraulic Energy to Dramatically Improve Lateral Reach

Optimising Hydraulic Energy to Dramatically Improve Lateral Reach Optimising Hydraulic Energy to Dramatically Improve Lateral Reach What Affects Reach? Build angle Size of completion CT size Drag Mechanical Fluid Debris in well BHA size End load CT size End load Buoyancy

More information

HPHT Annular Casing Packer. Obex Annular Casing Packer

HPHT Annular Casing Packer. Obex Annular Casing Packer HPHT Annular Casing Packer Obex Annular Casing Packer Industry Challenge Casing packer to support second stage cement Reduce hydrostatic pressure on formation Get cement to surface Annular gas migration

More information

W I L D W E L L C O N T R O L AIR DRILLING

W I L D W E L L C O N T R O L AIR DRILLING AIR DRILLING Air Drilling Learning Objectives You will learn the basics of: Air drilling equipment Types of air drilling Differences between mud and air drilling You will learn how to apply well control

More information

Blowout during Workover Operation A case study Narration by: Tarsem Singh & Arvind Jain, OISD

Blowout during Workover Operation A case study Narration by: Tarsem Singh & Arvind Jain, OISD 1. Introduction An incident of gas leakage from a well took place during workover operations. Subsequently, the gas caught fire on the fourth day in which twelve persons were injured. Two contract workers,

More information

North American sealing solutions Bridge Plug Ball Drop Frac Plug Caged Ball Frac Plug

North American sealing solutions Bridge Plug Ball Drop Frac Plug Caged Ball Frac Plug North American sealing solutions Bridge Plug Ball Drop Frac Plug Caged Ball Frac Plug The North American Sealing Solutions composite bridge plug, caged ball and ball drop (flow thru) frac plug provide

More information

Elevation Resources DAILY OPERATIONS. Clean and prep location, MIRU pulling unit to mill liner top

Elevation Resources DAILY OPERATIONS. Clean and prep location, MIRU pulling unit to mill liner top DAYS FROM SPUD: 35 DAYS ON 0 Mar 1 2016 RIG SUPERVISOR: Tyler Clean and prep location, MIRU pulling unit to mill liner top Blade location, set anchors. Bring surface and int CSG valves to surface and fill

More information

ECD Reduction Tool. R. K. Bansal, Brian Grayson, Jim Stanley Control Pressure Drilling & Testing

ECD Reduction Tool. R. K. Bansal, Brian Grayson, Jim Stanley Control Pressure Drilling & Testing ECD Reduction Tool R. K. Bansal, Brian Grayson, Jim Stanley Control Pressure Drilling & Testing Drilling Engineering Association, Fourth Quarter Meeting November 20, 2008 1 Presentation outline Description

More information

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG RAILROAD COMMISSION OF TEXAS 1701 N. Congress P.O. Box 12967 Austin, Texas 78701-2967 Status: Form W-2 OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG Date: Tracking No.: Approved 06/29/2015

More information

Type 967 Diamond Broaching Type 968 Sidewinder reamer shoe

Type 967 Diamond Broaching Type 968 Sidewinder reamer shoe Type 965 float collar Type 966 float shoe 1. GENERAL INFORMATION & RECOMMENDATIONS Type 967 Diamond Broaching Type 968 Sidewinder reamer shoe Type 969 Sidewinder reamer shoe Float Equipment Top-Co Float

More information

Float Equipment TYPE 925/926

Float Equipment TYPE 925/926 Type 925 Float Collar Plunger Valve Float Equipment For less demanding well conditions, such as shallower depths or lower pressures, Top- Co offers economical float equipment certified to API RP 10F category

More information

A New and Simplified Method for Determination of Conductor Surface Casing Setting Depths in Shallow Marine Sediments (SMS)

A New and Simplified Method for Determination of Conductor Surface Casing Setting Depths in Shallow Marine Sediments (SMS) AADE-07-NTCE-41 A New and Simplified Method for Determination of Conductor Surface Casing Setting Depths in Shallow Marine Sediments (SMS) Paknejad, A., Texas A&M University; Schubert, J., Texas A&M University

More information

Debris Management Drilling Tools

Debris Management Drilling Tools Debris Management Drilling Tools Protecting BHA components during well construction Remove drilling debris from the wellbore before it creates expensive problems. Debris commonly causes downhole tool failure,

More information

Hydraulic Optimization Worksheet for MS Excel All Versions subsequent to 5.0

Hydraulic Optimization Worksheet for MS Excel All Versions subsequent to 5.0 Hydraulic Optimization Worksheet for MS Excel All Versions subsequent to 5.0 1. Introduction. 2. Data Input. Header. Bit Information. Mud Information. Casing Program. P.D.M./Turbine. Drill String Design.

More information

Operations planning for optimal hole cleaning

Operations planning for optimal hole cleaning Operations planning for optimal hole cleaning Rev 1.0 14 th March 2004. Technical comments? info@kingdomdrilling.co.uk Page 1 Table of contents Operations planning for optimal hole cleaning... 1 Table

More information

RPSEA UDW Forum June 22 & 23, Secure Energy for America

RPSEA UDW Forum June 22 & 23, Secure Energy for America RPSEA UDW Forum June 22 & 23, 2010 Secure Energy for America PROJECT TEAM RPSEA Operator Advisory Committee Anadarko Chevron Shell ConocoPhillips Subcontractors IntecSea NOV CTES General Marine Contractors

More information

SPE/IADC Abstract

SPE/IADC Abstract SPE/IADC 125311 Pressurized Mud Cap Drilling Drastically Reduces Non-Productive Time in Soka Field, South Sumatera Michael Runtuwene, Sanny Suprihono, and Dany Rizka, SPE, Medco E&P Indonesia, Andi Eka

More information

Hard or Soft Shut-in : Which is the Best Approach?

Hard or Soft Shut-in : Which is the Best Approach? HARD - SOFT shut-in? Hard or Soft Shut-in : Which is the Best Approach? March '93 INTRODUCTION There is now reasonable acceptance through-out the industry for the use of a hard shut-in procedure following

More information

Oil Well Potential Test, Completion or Recompletion Report, and Log

Oil Well Potential Test, Completion or Recompletion Report, and Log Tracking No.: 102948 Status: Submitted RAILROAD COMMISSION OF TEXAS Oil and Gas Division API No. 42- Oil Well Potential Test, Completion or Recompletion Report, and Log 1. FIELD NAME (as per RRC Records

More information

Air and Gas Drilling

Air and Gas Drilling Air and Gas Drilling Air and Gas Drilling It is a technique in which the more common drilling fluids, (water or mud) are replaced by highly compressible Air or Natural gas. But Compressibility makes pressure

More information

R.K. Bansal, Weatherford; P.A. Bern, BP Exploration; Rick Todd, Weatherford; R.V. Baker, BP America; Tom Bailey, Weatherford

R.K. Bansal, Weatherford; P.A. Bern, BP Exploration; Rick Todd, Weatherford; R.V. Baker, BP America; Tom Bailey, Weatherford AADE-07-NTCE-69 A Downhole Tool for Reducing ECD R.K. Bansal, Weatherford; P.A. Bern, BP Exploration; Rick Todd, Weatherford; R.V. Baker, BP America; Tom Bailey, Weatherford Copyright 2007, AADE This paper

More information

SYSTEMIC APPROACH TO MINIMIZE STUCK PIPE INCIDENTS IN OIL WELLS

SYSTEMIC APPROACH TO MINIMIZE STUCK PIPE INCIDENTS IN OIL WELLS Journal of Al Azhar University Engineering Sector Vol. 11, No. 38, January, 2016, 255-264 SYSTEMIC APPROACH TO MINIMIZE STUCK PIPE INCIDENTS IN OIL WELLS H. Abd Elsalam 1, Y. ElNady 2, T. Elfakharany 2

More information

NeoProducts, LLC 1201 Dealers Ave. Harahan, LA Ph:

NeoProducts, LLC 1201 Dealers Ave. Harahan, LA Ph: Please read this entire document. It concerns all 9⅝ Vented Thru-tubing Bridge Plugs Read this document before proceeding to NeoProducts Recommended Best Practices for 9⅝ vented T- TBPs. Whenever running

More information

H. H. HOWELL, INC. Inland Ocean Bevans #1 Bevans & Wildcat Field Menard County, Texas

H. H. HOWELL, INC. Inland Ocean Bevans #1 Bevans & Wildcat Field Menard County, Texas H. H. HOWELL, INC. Bevans & Wildcat Field Menard County, Texas API #42-327- 31235 RRC Permit # 803460 GAU letter, RRC Letter #GAU-1436 = 245 Ground Elevation GL: 2186 (Rig KB to GL =8 ) Rig KB =2194 Location:

More information

BLACK HILLS PLATEAU PRODUCTION COMPANY

BLACK HILLS PLATEAU PRODUCTION COMPANY BLACK HILLS PLATEAU PRODUCTION COMPANY DRILLING PROGRAM Homer Deep Unit 9 11CH SHL: 300 FNL, 200 FWL, NWNW Sect. 9 T8S R98W BHL: 1350 FSL, 2100 FEL NWSE Sect. 15 T8S R98W Garfield & Mesa Counties, Colorado

More information

DRILLING MANAGED PRESSURE REGIONAL OUTLOOK: EAST AFRICA REDUCED EMISSION COMPLETIONS SHALE TECHNOLOGY REVIEW

DRILLING MANAGED PRESSURE REGIONAL OUTLOOK: EAST AFRICA REDUCED EMISSION COMPLETIONS SHALE TECHNOLOGY REVIEW MARCH 2014 / DEFINING TECHNOLOGY FOR EXPLORATION, DRILLING AND PRODUCTION / WorldOil.com MANAGED PRESSURE DRILLING How automated MPD enables drilling of an impossible well in Mexico REGIONAL OUTLOOK: EAST

More information

MPD Technique in Haynesville Shale Delivers Significant Value in Over Pressured Zones, A Case Study on Four Wells.

MPD Technique in Haynesville Shale Delivers Significant Value in Over Pressured Zones, A Case Study on Four Wells. AADE-11-NTCE-55 MPD Technique in Haynesville Shale Delivers Significant Value in Over Pressured Zones, A Case Study on Four Wells. Serkan Cenberlitas, Jim Crenshaw, and Ferhat Gumus, Weatherford International;

More information

Extended leak off testing

Extended leak off testing Extended leak off testing Rev: 1.0 03/01/01 Purpose To ensure minimal operational time and risk exposure to personnel, process, production and equipment. The following extended leak off test procedures

More information

Dilution-Based Dual Gradient Well Control. Presented at the 2011 IADC Dual Gradient Workshop, 5 May 2011 by Paul Boudreau, Dual Gradient Systems LLC

Dilution-Based Dual Gradient Well Control. Presented at the 2011 IADC Dual Gradient Workshop, 5 May 2011 by Paul Boudreau, Dual Gradient Systems LLC Dilution-Based Dual Gradient Well Control Presented at the 2011 IADC Dual Gradient Workshop, 5 May 2011 by Paul Boudreau, Dual Gradient Systems LLC In this very short presentation, we will Review Dilution-based

More information

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG RAILROAD COMMISSION OF TEXAS 1701 N. Congress P.O. Box 12967 Austin, Texas 78701-2967 Status: Form W-2 OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG Date: Tracking.: Approved 03/11/2015

More information

IADC/SPE Innovative Tubular, Hoisting, and Deepwater Rig Designs Extend Hook Load Envelope to 2,000,000 Pounds

IADC/SPE Innovative Tubular, Hoisting, and Deepwater Rig Designs Extend Hook Load Envelope to 2,000,000 Pounds IADC/SPE151140 Innovative Tubular, Hoisting, and Deepwater Rig Designs Extend Hook Load Envelope to 2,000,000 Pounds J. N. Brock, R. B. Chandler, NOV Grant Prideco; C. Selen, Maersk Drilling USA; J. Dugas,

More information

Offshore Managed Pressure Drilling Experiences in Asia Pacific. SPE paper

Offshore Managed Pressure Drilling Experiences in Asia Pacific. SPE paper Offshore Managed Pressure Drilling Experiences in Asia Pacific SPE paper 119875 Authors: Steve Nas, Shaun Toralde, Chad Wuest, SPE, Weatherford Solutions Sdn Bhd, SPE, Weatherford Indonesia SPE, Weatherford

More information

NOT TO COPY -- NO DISSEMINATE WITHOUT WRITTEN AGREEMENT. Presentation JB AG JCN JR 1

NOT TO COPY -- NO DISSEMINATE WITHOUT WRITTEN AGREEMENT. Presentation JB AG JCN JR 1 Presentation JB AG JCN JR 1 Presentation JB AG JCN JR 2 RIG TYPES Land rigs in 2012... total (approx) 3200 Jack Up,... in 2012... total (approx) 485 units 300 * in drilling mode 130 for WD > 350 ft Floaters,...

More information

Oman Central Gas Velocity Strings in deep tight gas wells. September th European Conference on Gas Well Deliquification.

Oman Central Gas Velocity Strings in deep tight gas wells. September th European Conference on Gas Well Deliquification. Oman Central Gas Velocity Strings in deep tight gas wells September 2009-4th European Conference on Gas Well Deliquification. Velocity Strings Oman Central Gas Agenda: - Objectives - Completions - VS design

More information

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG RAILROAD COMMISSION OF TEXAS 1701 N. Congress P.O. Box 12967 Austin, Texas 78701-2967 Status: Form W-2 OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG Date: Tracking No.: Approved 03/16/2016

More information

Safety and Risk Engineering. HSE Case Implementation Clive Rawson

Safety and Risk Engineering. HSE Case Implementation Clive Rawson Safety and Risk Engineering HSE Case Implementation Clive Rawson Purpose ALARP Risk Assessment Major Accident Events Bowties Safety Critical Systems Performance Standards Implementation Getting HSE Case

More information

Coiled Tubing string Fatigue Management in High Pressure Milling Operation- Case Study

Coiled Tubing string Fatigue Management in High Pressure Milling Operation- Case Study Coiled Tubing string Fatigue Management in High Pressure Milling Operation- Case Study Abstract: Paper Presenter: Ebrahim Rabbani 1 e.rabbani@mehranservices.com Ebrahim Rabbani, Danial Davoodi 2, Fatemeh

More information

Abandonment Program for Paramount Fort Liard F 36

Abandonment Program for Paramount Fort Liard F 36 Abandonment Program for Paramount Fort Liard F 36 Well Name: Paramount et al Liard F 36 Area: 60 0 10 N, 123 0 15 W Location: Latitude: 60 0 05 27 Longitude: 123 0 22 00 UWI: 300F366010123150 WID: 1841

More information

Understanding pressure and pressure

Understanding pressure and pressure CHAPTER 1 1-1 PRESSURE BASICS Remember to think downhole. The concepts provided in this section cover the foundations for good well control. Understanding pressure and pressure relationships is important

More information

Zarvona Energy LLC DAILY OPERATIONS

Zarvona Energy LLC DAILY OPERATIONS DAYS FROM SPUD: 120 DAYS ON 0 Jun 28 2016 RIG SUPERVISOR: Tyler Dupriest MIRU pulling unit MIRU pulling unit, move in and tally TBG. SDFN RIH with RBP DAYS FROM SPUD: 121 DAYS ON 1 Jun 29 2016 RIG SUPERVISOR:

More information

Live well deployment of long perforating gun system using combined CT technologies

Live well deployment of long perforating gun system using combined CT technologies Live well deployment of long perforating gun system using combined CT technologies SPE ICoTA European Well Intervention Conference Aberdeen - 12 November, 2014 Simon Smith, Technical Support Manager Baker

More information

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG

RAILROAD COMMISSION OF TEXAS OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG RAILROAD COMMISSION OF TEXAS 1701 N. Congress P.O. Box 12967 Austin, Texas 78701-2967 Status: Date: Tracking No.: Form W-2 OIL WELL POTENTIAL TEST, COMPLETION OR RECOMPLETION REPORT, AND LOG Submitted

More information

SURFACE CASING SELECTION FOR COLLAPSE, BURST AND AXIAL DESIGN FACTOR LOADS EXERCISE

SURFACE CASING SELECTION FOR COLLAPSE, BURST AND AXIAL DESIGN FACTOR LOADS EXERCISE SURFACE CASING SELECTION FOR COLLAPSE, BURST AND AXIAL DESIGN FACTOR LOADS EXERCISE Instructions Use the example well data from this document or the powerpoint notes handout to complete the following graphs.

More information

DB Bridge Plug. Features. Benefits. Applications

DB Bridge Plug. Features. Benefits. Applications DB Bridge Plug The WELLFIRST Premium Cast Iron Bridge Plug designed to run on electric line. Rated between 2000-10000-psi differential, and 300 F from above and below. Features Field Proven Design Constructed

More information

W I L D W E L L C O N T R O L PRESSURE BASICS AND CONCEPTS

W I L D W E L L C O N T R O L PRESSURE BASICS AND CONCEPTS PRESSURE BASICS AND CONCEPTS Pressure Basics and Concepts Learning Objectives You will be familiarized with the following basic pressure concepts: Defining pressure Hydrostatic pressure Pressure gradient

More information

The Developing Design of the Blowout Preventer in Deep Water

The Developing Design of the Blowout Preventer in Deep Water The Developing Design of the Blowout Preventer in Deep Water IADC World Drilling 2011 Conference & Exhibition 15-16 June 2011, Bella Centre, Copenhagen Eric Brown Project Manager National Oilwell Varco

More information